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IAC Assessment: OR0049
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IAC Assessment: OR0049
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IAC Center Oregon State University
Assessment Year 1989
Principal Product HARDWOOD & PALLET LUMBER
NAICS n/a
SIC 2421 - Sawmills And Planing Mills, General
Sales $10,000,000-$50,000,000
# of Employees 140
Plant Area (Sq.Ft.) 0
Annual Production 62,000 Thousand Feet
Production Hrs. Annual 8,736
Location (State) OR
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $251,430 9,285,463 kWh $0.03
Natural Gas $64,088 10,943 MMBtu $5.86
TOTAL ENERGY COSTS $315,518
RECOMMENDED SAVINGS* $42,841 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $40,071
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.6232 INSTALL SET-BACK TIMERS Savings:
$25,856
Cost:
-
$17,277 639,801 - - $8,579 - $17,277
639,801
kWh
-
-
MMBtu
$8,579
-
$
02: 2.3212 OPTIMIZE PLANT POWER FACTOR Savings:
$12,480
Cost:
$10,000
$12,480 - - - - - $12,480
-
kWh
-
-
MMBtu
-
-
$
03: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$607
Cost:
$500
- - $607 104 - - -
-
kWh
$607
104
MMBtu
-
-
$
04: 2.2122 INSTALL / REPAIR INSULATION ON CONDENSATE LINES Savings:
$2,770
Cost:
$3,720
- - $2,770 473 - - -
-
kWh
$2,770
473
MMBtu
-
-
$
05: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$132
Cost:
$206
$132 4,982 - - - - $132
4,982
kWh
-
-
MMBtu
-
-
$
06: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$996
Cost:
$2,000
$996 36,928 - - - - $996
36,928
kWh
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$42,841
Cost:
$16,426
$30,885 681,711 $3,377 577 $8,579 - $30,885
681,711
kWh
$3,377
577
MMBtu
$8,579
-
$
TOTAL IMPLEMENTED Savings:
$40,071
Cost:
$12,706
$30,885 681,711 $607 104 $8,579 - $30,885
681,711
kWh
$607
104
MMBtu
$8,579
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes