Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Oregon State University |
---|---|
Assessment Year | 1992 |
Principal Product | RANDOM WIDTH HARDWOOD |
NAICS | n/a |
SIC | 2426 - Hardwood Dimension & Flooring Mills |
Sales | $5,000,000-$10,000,000 |
# of Employees | 130 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 30,000 Thousand Feet |
Production Hrs. Annual | 4,160 |
Location (State) | WA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $217,434 | 7,423,798 | kWh | $0.03 |
Natural Gas | $248,996 | 82,977 | MMBtu | $3.00 |
TOTAL ENERGY COSTS | $466,430 | |||
RECOMMENDED SAVINGS* | $20,742 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $4,026 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.6232 INSTALL SET-BACK TIMERS |
Savings: $645 Cost: - |
$423 | 20,809 | - | - | $222 | - |
$423 20,809 kWh |
- - MMBtu |
$222 - $ |
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02: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $1,041 Cost: - |
$1,041 | 33,705 | - | - | - | - |
$1,041 33,705 kWh |
- - MMBtu |
- - $ |
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03: 2.7111 REDUCE ILLUMINATION TO MINIMUM NECESSARY LEVELS |
Savings: $1,813 Cost: $885 |
$1,603 | 54,220 | - | - | $210 | - |
$1,603 54,220 kWh |
- - MMBtu |
$210 - $ |
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04: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $440 Cost: $500 |
$440 | 17,585 | - | - | - | - |
$440 17,585 kWh |
- - MMBtu |
- - $ |
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05: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $636 Cost: $1,000 |
- | - | $636 | 793 | - | - |
- - kWh |
$636 793 MMBtu |
- - $ |
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06: 2.2123 INSULATE FEEDWATER TANK |
Savings: $157 Cost: $333 |
- | - | $157 | 196 | - | - |
- - kWh |
$157 196 MMBtu |
- - $ |
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07: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $2,119 Cost: $5,950 |
$2,119 | 86,460 | - | - | - | - |
$2,119 86,460 kWh |
- - MMBtu |
- - $ |
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08: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $536 Cost: $8,869 |
$536 | 17,878 | - | - | - | - |
$536 17,878 kWh |
- - MMBtu |
- - $ |
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09: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $13,355 Cost: $66,726 |
$13,355 | 656,506 | - | - | - | - |
$13,355 656,506 kWh |
- - MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $20,742 Cost: $84,263 |
$19,517 | 887,163 | $793 | 989 | $432 | - | $19,517 887,163 kWh |
$793 989 MMBtu |
$432 - $ |
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TOTAL IMPLEMENTED |
Savings: $4,026 Cost: $10,754 |
$3,180 | 105,803 | $636 | 793 | $210 | - | $3,180 105,803 kWh |
$636 793 MMBtu |
$210 - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |