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IAC Assessment: SD0419
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IAC Assessment: SD0419
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Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
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IAC Center San Diego State University
Assessment Year 2009
Principal Product Mayonnaise, Dressing, and Other Prepared Sauce Manufacturin
NAICS 311941 - Mayonnaise, Dressing, and Other Prepared Sauce Manufacturing
SIC 2035 - Pickles, Sauces, And Salad Dressings
Sales <$500,000
# of Employees 400
Plant Area (Sq.Ft.) 680,000
Annual Production 700,000,000 Pounds
Production Hrs. Annual 3,250
Location (State) CA
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $1,390,034 16,641,007 kWh $0.08
Electricity Demand $532,051 33,909 kW-months/year $15.69
Electricity Fees $11,682 - $ -
Natural Gas $265,670 32,915 MMBtu $8.07
TOTAL ENERGY COSTS $2,199,437
RECOMMENDED SAVINGS* $157,663 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $95,815
#|Description Savings
Cost
Status Electricity Usage Electricity Demand Natural Gas Electricity Usage Electricity Demand Natural Gas
$ kWh $ kW-months/year $ MMBtu
01: 2.7241 INSTALL OUTSIDE AIR DAMPER / ECONOMIZER ON HVAC UNIT Savings:
$17,800
Cost:
$10,000
$17,800 213,000 - - - - $17,800
213,000
kWh
-
-
kW-months/year
-
-
MMBtu
02: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED Savings:
$12,170
Cost:
$1,000
$8,938 107,000 $3,232 206 - - $8,938
107,000
kWh
$3,232
206
kW-months/year
-
-
MMBtu
03: 2.1243 USE HEAT FROM BOILER BLOWDOWN TO PREHEAT BOILER FEED WATER Savings:
$7,840
Cost:
$10,000
- - - - $7,840 937 -
-
kWh
-
-
kW-months/year
$7,840
937
MMBtu
04: 2.2121 INCREASE AMOUNT OF CONDENSATE RETURNED Savings:
$15,940
Cost:
$2,263
$15,940 328,250 - - - - $15,940
328,250
kWh
-
-
kW-months/year
-
-
MMBtu
05: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$49,905
Cost:
$161,162
$36,716 437,100 $13,189 840 - - $36,716
437,100
kWh
$13,189
840
kW-months/year
-
-
MMBtu
06: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$39,102
Cost:
$50,136
$39,102 465,505 - - - - $39,102
465,505
kWh
-
-
kW-months/year
-
-
MMBtu
07: 2.7261 INSTALL TIMERS AND/OR THERMOSTATS Savings:
$14,906
Cost:
$500
$14,906 177,450 - - - - $14,906
177,450
kWh
-
-
kW-months/year
-
-
MMBtu
TOTAL RECOMMENDED Savings:
$157,663
Cost:
$235,061
$133,402 1,728,305 $16,421 1,046 $7,840 937 $133,402
1,728,305
kWh
$16,421
1,046
kW-months/year
$7,840
937
MMBtu
TOTAL IMPLEMENTED Savings:
$95,815
Cost:
$174,425
$79,394 1,085,350 $16,421 1,046 - - $79,394
1,085,350
kWh
$16,421
1,046
kW-months/year
-
-
MMBtu
Savings
Cost
$ kWh $ kW-months/year $ MMBtu
Electricity Usage Electricity Demand Natural Gas Electricity Usage Electricity Demand Natural Gas