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IAC Assessment: SF0043
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IAC Assessment: SF0043
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IAC Center San Francisco State University
Assessment Year 1994
Principal Product Roasted Coffee
NAICS n/a
SIC 2095 - Roasted Coffee
Sales $100,000,000-$500,000,000
# of Employees 400
Plant Area (Sq.Ft.) 42,000
Annual Production 40,000 Tons
Production Hrs. Annual 4,800
Location (State) CA
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $738,118 10,025,498 kWh $0.07
Natural Gas $236,907 82,915 MMBtu $2.86
TOTAL ENERGY COSTS $975,025
RECOMMENDED SAVINGS* $45,223 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* -
#|Description Savings
Cost
Status Electricity Usage Natural Gas Electricity Usage Natural Gas
$ kWh $ MMBtu
01: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$3,044
Cost:
$2,794
$3,044 41,325 - - $3,044
41,325
kWh
-
-
MMBtu
02: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$3,403
Cost:
$9,820
$3,403 46,307 - - $3,403
46,307
kWh
-
-
MMBtu
03: 2.7135 INSTALL OCCUPANCY SENSORS Savings:
$2,561
Cost:
$1,608
$2,561 34,877 - - $2,561
34,877
kWh
-
-
MMBtu
04: 2.4314 USE SYNTHETIC LUBRICANT Savings:
$2,093
Cost:
-
$2,093 28,429 - - $2,093
28,429
kWh
-
-
MMBtu
05: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$1,020
Cost:
$250
$1,020 13,775 - - $1,020
13,775
kWh
-
-
MMBtu
06: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$4,273
Cost:
$3,317
$4,273 58,030 - - $4,273
58,030
kWh
-
-
MMBtu
07: 2.4323 USE OPTIMUM SIZE AND CAPACITY EQUIPMENT Savings:
$3,427
Cost:
$2,665
- - $3,427 1,590 -
-
kWh
$3,427
1,590
MMBtu
08: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$7,772
Cost:
$10,800
$7,772 105,510 - - $7,772
105,510
kWh
-
-
MMBtu
09: 2.1213 DIRECT WARMEST AIR TO COMBUSTION INTAKE Savings:
$11,302
Cost:
$3,350
- - $11,302 4,067 -
-
kWh
$11,302
4,067
MMBtu
10: 2.4323 USE OPTIMUM SIZE AND CAPACITY EQUIPMENT Savings:
$6,328
Cost:
$550
- - $6,328 2,930 -
-
kWh
$6,328
2,930
MMBtu
TOTAL RECOMMENDED Savings:
$45,223
Cost:
$35,154
$24,166 328,253 $21,057 8,587 $24,166
328,253
kWh
$21,057
8,587
MMBtu
TOTAL IMPLEMENTED Savings:
-
Cost:
-
- - - - -
-
kWh
-
-
MMBtu
Savings
Cost
$ kWh $ MMBtu
Electricity Usage Natural Gas Electricity Usage Natural Gas