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IAC Assessment: SF0050
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IAC Assessment: SF0050
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IAC Center San Francisco State University
Assessment Year 1995
Principal Product Corrugated Cartons
NAICS n/a
SIC 2653 - Corrugated And Solid Fiber Boxes
Sales $50,000,000-$100,000,000
# of Employees 190
Plant Area (Sq.Ft.) 435,600
Annual Production 100,000 Tons
Production Hrs. Annual 7,238
Location (State) CA
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $765,297 8,568,582 kWh $0.09
Natural Gas $299,594 96,611 MMBtu $3.10
TOTAL ENERGY COSTS $1,064,891
RECOMMENDED SAVINGS* $565,986 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $56,203
#|Description Savings
Cost
Status Electricity Usage Natural Gas Electricity Usage Natural Gas
$ kWh $ MMBtu
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$48,642
Cost:
$166,900
$48,642 544,549 - - $48,642
544,549
kWh
-
-
MMBtu
02: 2.3212 OPTIMIZE PLANT POWER FACTOR Savings:
$3,578
Cost:
$5,911
$3,578 - - - $3,578
-
kWh
-
-
MMBtu
03: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$2,230
Cost:
$1,125
$2,230 24,912 - - $2,230
24,912
kWh
-
-
MMBtu
04: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$21,960
Cost:
$19,510
$21,960 245,897 - - $21,960
245,897
kWh
-
-
MMBtu
05: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES Savings:
$1,254
Cost:
$748
- - $1,254 409 -
-
kWh
$1,254
409
MMBtu
06: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS Savings:
$401
Cost:
$81
- - $401 129 -
-
kWh
$401
129
MMBtu
07: 2.1243 USE HEAT FROM BOILER BLOWDOWN TO PREHEAT BOILER FEED WATER Savings:
$4,773
Cost:
$25,000
- - $4,773 1,526 -
-
kWh
$4,773
1,526
MMBtu
08: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$4,930
Cost:
$900
- - $4,930 188 -
-
kWh
$4,930
188
MMBtu
09: 2.3415 USE A FOSSIL FUEL ENGINE TO COGENERATE ELECTRICITY OR MOTIVE POWER; AND UTILIZE HEAT Savings:
$478,218
Cost:
$653,645
$707,157 7,962,192 $(-228,939) (-73,828) $707,157
7,962,192
kWh
$(-228,939)
(-73,828)
MMBtu
TOTAL RECOMMENDED Savings:
$565,986
Cost:
$873,820
$783,567 8,777,550 $(-217,581) (-71,576) $783,567
8,777,550
kWh
$(-217,581)
(-71,576)
MMBtu
TOTAL IMPLEMENTED Savings:
$56,203
Cost:
$169,006
$50,872 569,461 $5,331 317 $50,872
569,461
kWh
$5,331
317
MMBtu
Savings
Cost
$ kWh $ MMBtu
Electricity Usage Natural Gas Electricity Usage Natural Gas