Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | San Francisco State University |
---|---|
Assessment Year | 1995 |
Principal Product | Corrugated Cartons |
NAICS | n/a |
SIC | 2653 - Corrugated And Solid Fiber Boxes |
Sales | $50,000,000-$100,000,000 |
# of Employees | 190 |
Plant Area (Sq.Ft.) | 435,600 |
Annual Production | 100,000 Tons |
Production Hrs. Annual | 7,238 |
Location (State) | CA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $765,297 | 8,568,582 | kWh | $0.09 |
Natural Gas | $299,594 | 96,611 | MMBtu | $3.10 |
TOTAL ENERGY COSTS | $1,064,891 | |||
RECOMMENDED SAVINGS* | $565,986 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $56,203 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $48,642 Cost: $166,900 |
$48,642 | 544,549 | - | - |
$48,642 544,549 kWh |
- - MMBtu |
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02: 2.3212 OPTIMIZE PLANT POWER FACTOR |
Savings: $3,578 Cost: $5,911 |
$3,578 | - | - | - |
$3,578 - kWh |
- - MMBtu |
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03: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $2,230 Cost: $1,125 |
$2,230 | 24,912 | - | - |
$2,230 24,912 kWh |
- - MMBtu |
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04: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $21,960 Cost: $19,510 |
$21,960 | 245,897 | - | - |
$21,960 245,897 kWh |
- - MMBtu |
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05: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $1,254 Cost: $748 |
- | - | $1,254 | 409 |
- - kWh |
$1,254 409 MMBtu |
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06: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $401 Cost: $81 |
- | - | $401 | 129 |
- - kWh |
$401 129 MMBtu |
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07: 2.1243 USE HEAT FROM BOILER BLOWDOWN TO PREHEAT BOILER FEED WATER |
Savings: $4,773 Cost: $25,000 |
- | - | $4,773 | 1,526 |
- - kWh |
$4,773 1,526 MMBtu |
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08: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $4,930 Cost: $900 |
- | - | $4,930 | 188 |
- - kWh |
$4,930 188 MMBtu |
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09: 2.3415 USE A FOSSIL FUEL ENGINE TO COGENERATE ELECTRICITY OR MOTIVE POWER; AND UTILIZE HEAT |
Savings: $478,218 Cost: $653,645 |
$707,157 | 7,962,192 | $(-228,939) | (-73,828) |
$707,157 7,962,192 kWh |
$(-228,939) (-73,828) MMBtu |
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TOTAL RECOMMENDED |
Savings: $565,986 Cost: $873,820 |
$783,567 | 8,777,550 | $(-217,581) | (-71,576) | $783,567 8,777,550 kWh |
$(-217,581) (-71,576) MMBtu |
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TOTAL IMPLEMENTED |
Savings: $56,203 Cost: $169,006 |
$50,872 | 569,461 | $5,331 | 317 | $50,872 569,461 kWh |
$5,331 317 MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |