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IAC Assessment: SU0349
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IAC Assessment: SU0349
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IAC Center Syracuse University
Assessment Year 2013
Principal Product CCD Sensors
NAICS 334413 - Semiconductor and Related Device Manufacturing
SIC 3674 - Semiconductors And Related Devices
Sales $10,000,000-$50,000,000
# of Employees 250
Plant Area (Sq.Ft.) 263,000
Annual Production 250,000 Pieces
Production Hrs. Annual 6,240
Location (State) NY
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $1,930,427 21,397,000 kWh $0.09
Electricity Fees $255,426 - $ -
TOTAL ENERGY COSTS $2,536,752
RECOMMENDED SAVINGS* $1,281,892 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $9,811
#|Description Savings
Cost
Status Electricity Usage Natural Gas One-time Revenue or Avoided Cost Electricity Usage Natural Gas One-time Revenue or Avoided Cost
$ kWh $ MMBtu $ $
01: 4.821 PAY BILLS ON TIME TO AVOID LATE FEES Savings:
$6,610
Cost:
-
- - - - $6,610 - -
-
kWh
-
-
MMBtu
$6,610
-
$
02: 2.4226 USE / PURCHASE OPTIMUM SIZED COMPRESSOR Savings:
$20,356
Cost:
$4,000
$(-14,770) (-164,112) - - $35,126 - $(-14,770)
(-164,112)
kWh
-
-
MMBtu
$35,126
-
$
03: 2.4221 INSTALL COMPRESSOR AIR INTAKES IN COOLEST LOCATIONS Savings:
$4,244
Cost:
$2,033
$4,244 47,156 - - - - $4,244
47,156
kWh
-
-
MMBtu
-
-
$
04: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$457
Cost:
$216
$87 963 - - $370 - $87
963
kWh
-
-
MMBtu
$370
-
$
05: 2.2628 UTILIZE A LESS EXPENSIVE COOLING METHOD Savings:
$882,762
Cost:
$552,244
$(-272,938) (-3,032,640) - - $1,155,700 - $(-272,938)
(-3,032,640)
kWh
-
-
MMBtu
$1,155,700
-
$
06: 2.1392 REPLACE PURCHASED STEAM WITH OTHER ENERGY SOURCE Savings:
$361,538
Cost:
$453,062
- - $(-713,405) (-101,915) $1,074,943 - -
-
kWh
$(-713,405)
(-101,915)
MMBtu
$1,074,943
-
$
07: 3.1161 ELIMINATE/REDUCE AN OPERATION Savings:
$2,724
Cost:
$5,760
$(-66) (-732) - - $2,790 - $(-66)
(-732)
kWh
-
-
MMBtu
$2,790
-
$
08: 2.4321 UPGRADE OBSOLETE EQUIPMENT Savings:
$3,201
Cost:
$8,460
$3,201 35,568 - - - - $3,201
35,568
kWh
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$1,281,892
Cost:
$1,025,775
$(-280,242) (-3,113,797) $(-713,405) (-101,915) $2,275,539 - $(-280,242)
(-3,113,797)
kWh
$(-713,405)
(-101,915)
MMBtu
$2,275,539
-
$
TOTAL IMPLEMENTED Savings:
$9,811
Cost:
$8,460
$3,201 35,568 - - $6,610 - $3,201
35,568
kWh
-
-
MMBtu
$6,610
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas One-time Revenue or Avoided Cost Electricity Usage Natural Gas One-time Revenue or Avoided Cost