Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Tennessee |
---|---|
Assessment Year | 1983 |
Principal Product | MILK,ICE CREAM & CHEESE |
NAICS | n/a |
SIC | 2026 - Fluid Milk |
Sales | $50,000,000-$100,000,000 |
# of Employees | 250 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 6,000 Thousand Gallons |
Production Hrs. Annual | 4,680 |
Location (State) | TN |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $679,127 | 14,924,971 | kWh | $0.05 |
Natural Gas | $169,025 | 39,456 | MMBtu | $4.28 |
TOTAL ENERGY COSTS | $848,152 | |||
RECOMMENDED SAVINGS* | $17,970 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | - |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.2444 USE HOT PROCESS FLUIDS TO PREHEAT INCOMING PROCESS FLUIDS |
Savings: $6,775 Cost: - |
$2,740 | 54,807 | $4,035 | 938 |
$2,740 54,807 kWh |
$4,035 938 MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $1,610 Cost: - |
$1,610 | 32,239 | - | - |
$1,610 32,239 kWh |
- - MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $7,822 Cost: - |
- | - | $7,822 | 1,819 |
- - kWh |
$7,822 1,819 MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
04: 3.1192 REDUCE SCRAP PRODUCTION |
Savings: $1,763 Cost: $2,000 |
- | - | $1,763 | 410 |
- - kWh |
$1,763 410 MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $17,970 Cost: $2,000 |
$4,350 | 87,046 | $13,620 | 3,167 | $4,350 87,046 kWh |
$13,620 3,167 MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: - Cost: - |
- | - | - | - | - - kWh |
- - MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |