Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Tennessee |
---|---|
Assessment Year | 1986 |
Principal Product | GOLF CLUBS |
NAICS | n/a |
SIC | 3949 - Sporting And Athletic Goods, Nec |
Sales | $10,000,000-$50,000,000 |
# of Employees | 350 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 1,650,000 Pieces |
Production Hrs. Annual | 3,760 |
Location (State) | TN |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $134,883 | 2,520,809 | kWh | $0.05 |
Natural Gas | $121,014 | 24,464 | MMBtu | $4.95 |
Fuel Oil #2 | $6,299 | 1,028 | MMBtu | $6.13 |
TOTAL ENERGY COSTS | $262,196 | |||
RECOMMENDED SAVINGS* | $26,935 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $11,066 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Fuel Oil #2 | Electricity Usage | Natural Gas | Fuel Oil #2 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $6,608 Cost: $4,408 |
- | - | $6,280 | 1,282 | $328 | 53 |
- - kWh |
$6,280 1,282 MMBtu |
$328 53 MMBtu |
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02: 2.2514 COVER OPEN TANKS |
Savings: $5,049 Cost: $650 |
- | - | $4,798 | 979 | $251 | 41 |
- - kWh |
$4,798 979 MMBtu |
$251 41 MMBtu |
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03: 2.2511 INSULATE BARE EQUIPMENT |
Savings: $4,465 Cost: $1,491 |
- | - | $4,243 | 865 | $222 | 37 |
- - kWh |
$4,243 865 MMBtu |
$222 37 MMBtu |
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04: 2.7243 IMPROVE AIR CIRCULATION WITH DESTRATIFICATION FANS / OTHER METHODS |
Savings: $4,415 Cost: $7,500 |
- | - | $4,194 | 856 | $221 | 36 |
- - kWh |
$4,194 856 MMBtu |
$221 36 MMBtu |
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05: 2.6122 ADJUST VENTS TO MINIMIZE ENERGY USE |
Savings: $3,340 Cost: - |
$3,340 | 63,013 | - | - | - | - |
$3,340 63,013 kWh |
- - MMBtu |
- - MMBtu |
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06: 2.2122 INSTALL / REPAIR INSULATION ON CONDENSATE LINES |
Savings: $529 Cost: $182 |
- | - | $503 | 102 | $26 | 5 |
- - kWh |
$503 102 MMBtu |
$26 5 MMBtu |
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07: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $1,025 Cost: $105 |
$1,025 | 19,343 | - | - | - | - |
$1,025 19,343 kWh |
- - MMBtu |
- - MMBtu |
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08: 2.6212 TURN OFF EQUIPMENT DURING BREAKS, REDUCE OPERATING TIME |
Savings: $737 Cost: $220 |
$737 | 13,775 | - | - | - | - |
$737 13,775 kWh |
- - MMBtu |
- - MMBtu |
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09: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $674 Cost: $240 |
$674 | 12,603 | - | - | - | - |
$674 12,603 kWh |
- - MMBtu |
- - MMBtu |
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10: 2.6212 TURN OFF EQUIPMENT DURING BREAKS, REDUCE OPERATING TIME |
Savings: $93 Cost: - |
$93 | 1,758 | - | - | - | - |
$93 1,758 kWh |
- - MMBtu |
- - MMBtu |
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TOTAL RECOMMENDED |
Savings: $26,935 Cost: $14,796 |
$5,869 | 110,492 | $20,018 | 4,084 | $1,048 | 172 | $5,869 110,492 kWh |
$20,018 4,084 MMBtu |
$1,048 172 MMBtu |
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TOTAL IMPLEMENTED |
Savings: $11,066 Cost: $4,513 |
$4,458 | 84,114 | $6,280 | 1,282 | $328 | 53 | $4,458 84,114 kWh |
$6,280 1,282 MMBtu |
$328 53 MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Fuel Oil #2 | Electricity Usage | Natural Gas | Fuel Oil #2 |