Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Dayton |
---|---|
Assessment Year | 1994 |
Principal Product | thermoplastic seals, pistons |
NAICS | n/a |
SIC | 3089 - Plastics Products, Nec |
Sales | $10,000,000-$50,000,000 |
# of Employees | 107 |
Plant Area (Sq.Ft.) | 42,000 |
Annual Production | 153,000,000 Pieces |
Production Hrs. Annual | 6,000 |
Location (State) | OH |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $1,914,000 | 29,427,316 | kWh | $0.07 |
Natural Gas | $18,636 | 3,860 | MMBtu | $4.83 |
TOTAL ENERGY COSTS | $1,932,636 | |||
RECOMMENDED SAVINGS* | $4,616 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $4,077 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.3131 RESCHEDULE PLANT OPERATIONS OR REDUCE LOAD TO AVOID PEAKS |
Savings: $1,026 Cost: - |
$1,026 | - | - | - | - | - |
$1,026 - kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 3.1191 CHANGE PROCEDURES / EQUIPMENT / OPERATING CONDITIONS |
Savings: $539 Cost: - |
$539 | - | - | - | - | - |
$539 - kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.7111 REDUCE ILLUMINATION TO MINIMUM NECESSARY LEVELS |
Savings: $3,051 Cost: $2,500 |
$3,403 | 154,162 | $(-1,532) | (-300) | $1,180 | - |
$3,403 154,162 kWh |
$(-1,532) (-300) MMBtu |
$1,180 - $ |
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TOTAL RECOMMENDED |
Savings: $4,616 Cost: $2,500 |
$4,968 | 154,162 | $(-1,532) | (-300) | $1,180 | - | $4,968 154,162 kWh |
$(-1,532) (-300) MMBtu |
$1,180 - $ |
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TOTAL IMPLEMENTED |
Savings: $4,077 Cost: $2,500 |
$4,429 | 154,162 | $(-1,532) | (-300) | $1,180 | - | $4,429 154,162 kWh |
$(-1,532) (-300) MMBtu |
$1,180 - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |