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IAC Assessment: UF0131
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IAC Assessment: UF0131
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IAC Center University of Florida
Assessment Year 1995
Principal Product Automobile Parts
NAICS n/a
SIC 3714 - Motor Vehicle Parts And Accessories
Sales $10,000,000-$50,000,000
# of Employees 250
Plant Area (Sq.Ft.) 140,000
Annual Production 150,000 Pieces
Production Hrs. Annual 4,550
Location (State) FL
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $455,573 6,830,305 kWh $0.07
Natural Gas $79,758 14,493 MMBtu $5.50
TOTAL ENERGY COSTS $535,331
RECOMMENDED SAVINGS* $223,481 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $100,422
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$6,967
Cost:
$13,352
$6,967 88,511 - - - - $6,967
88,511
kWh
-
-
MMBtu
-
-
$
02: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$2,319
Cost:
$204
$2,319 53,927 - - - - $2,319
53,927
kWh
-
-
MMBtu
-
-
$
03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$7,115
Cost:
$14,659
$7,115 75,029 - - - - $7,115
75,029
kWh
-
-
MMBtu
-
-
$
04: 2.7135 INSTALL OCCUPANCY SENSORS Savings:
$677
Cost:
$1,152
$677 19,930 - - - - $677
19,930
kWh
-
-
MMBtu
-
-
$
05: 2.7122 DISCONNECT BALLASTS Savings:
$553
Cost:
$1,400
$553 11,430 - - - - $553
11,430
kWh
-
-
MMBtu
-
-
$
06: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$1,001
Cost:
$1,116
$1,001 15,826 - - - - $1,001
15,826
kWh
-
-
MMBtu
-
-
$
07: 2.1321 REPLACE FOSSIL FUEL EQUIPMENT WITH ELECTRICAL EQUIPMENT Savings:
$8,226
Cost:
$11,400
$9,920 90,270 $(-1,694) (-308) - - $9,920
90,270
kWh
$(-1,694)
(-308)
MMBtu
-
-
$
08: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$845
Cost:
$350
$845 12,603 - - - - $845
12,603
kWh
-
-
MMBtu
-
-
$
09: 2.8114 CHANGE RATE SCHEDULES OR OTHER CHANGES IN UTILITY SERVICE Savings:
$110,283
Cost:
$250,000
- - - - $110,283 - -
-
kWh
-
-
MMBtu
$110,283
-
$
10: 3.6112 USE FILTER AND DRYING OVEN TO REDUCE SLUDGE VOLUME Savings:
$85,495
Cost:
$8,000
- - - - $85,495 - -
-
kWh
-
-
MMBtu
$85,495
-
$
TOTAL RECOMMENDED Savings:
$223,481
Cost:
$301,633
$29,397 367,526 $(-1,694) (-308) $195,778 - $29,397
367,526
kWh
$(-1,694)
(-308)
MMBtu
$195,778
-
$
TOTAL IMPLEMENTED Savings:
$100,422
Cost:
$36,361
$14,927 176,143 - - $85,495 - $14,927
176,143
kWh
-
-
MMBtu
$85,495
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes