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IAC Assessment: UM0002
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IAC Assessment: UM0002
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IAC Center University of Michigan
Assessment Year 1994
Principal Product Newspaper
NAICS n/a
SIC 2711 - Newspapers
Sales $10,000,000-$50,000,000
# of Employees 400
Plant Area (Sq.Ft.) 90,000
Annual Production 13,000 Tons
Production Hrs. Annual 1,800
Location (State) MI
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $228,159 3,702,521 kWh $0.06
Natural Gas $58,552 13,055 MMBtu $4.49
TOTAL ENERGY COSTS $286,711
RECOMMENDED SAVINGS* $34,815 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $24,146
#|Description Savings
Cost
Status Electricity Usage Natural Gas Electricity Usage Natural Gas
$ kWh $ MMBtu
01: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$6,833
Cost:
$8,340
$6,833 110,199 - - $6,833
110,199
kWh
-
-
MMBtu
02: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$17,313
Cost:
$58,573
$17,313 279,308 - - $17,313
279,308
kWh
-
-
MMBtu
03: 2.7135 INSTALL OCCUPANCY SENSORS Savings:
$1,961
Cost:
$2,330
$1,961 31,653 - - $1,961
31,653
kWh
-
-
MMBtu
04: 2.4226 USE / PURCHASE OPTIMUM SIZED COMPRESSOR Savings:
$4,332
Cost:
$7,600
$4,332 69,754 - - $4,332
69,754
kWh
-
-
MMBtu
05: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$720
Cost:
$2,000
$720 11,723 - - $720
11,723
kWh
-
-
MMBtu
06: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$2,881
Cost:
$1,000
- - $2,881 636 -
-
kWh
$2,881
636
MMBtu
07: 2.1222 INSTALL TURBULATORS Savings:
$775
Cost:
$1,400
- - $775 171 -
-
kWh
$775
171
MMBtu
TOTAL RECOMMENDED Savings:
$34,815
Cost:
$81,243
$31,159 502,637 $3,656 807 $31,159
502,637
kWh
$3,656
807
MMBtu
TOTAL IMPLEMENTED Savings:
$24,146
Cost:
$66,913
$24,146 389,507 - - $24,146
389,507
kWh
-
-
MMBtu
Savings
Cost
$ kWh $ MMBtu
Electricity Usage Natural Gas Electricity Usage Natural Gas