Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Wisconsin, Milwaukee |
---|---|
Assessment Year | 1988 |
Principal Product | CORRUGATED CONTAINERS |
NAICS | n/a |
SIC | 2653 - Corrugated And Solid Fiber Boxes |
Sales | $10,000,000-$50,000,000 |
# of Employees | 120 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 600,000 Thousand Feet |
Production Hrs. Annual | 6,000 |
Location (State) | WI |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $175,433 | 3,147,714 | kWh | $0.06 |
Natural Gas | $164,614 | 48,932 | MMBtu | $3.36 |
TOTAL ENERGY COSTS | $340,047 | |||
RECOMMENDED SAVINGS* | $45,809 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $35,594 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.4312 IMPROVE LUBRICATION PRACTICES |
Savings: $10,215 Cost: - |
$10,215 | 183,470 | - | - |
$10,215 183,470 kWh |
- - MMBtu |
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02: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $524 Cost: - |
$524 | 9,379 | - | - |
$524 9,379 kWh |
- - MMBtu |
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03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $4,890 Cost: $4,906 |
$4,890 | 87,925 | - | - |
$4,890 87,925 kWh |
- - MMBtu |
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04: 2.1311 REPLACE ELECTRICALLY-OPERATED EQUIPMENT WITH FOSSIL FUEL EQUIPMENT |
Savings: $2,044 Cost: $6,500 |
$2,751 | 49,531 | $(-707) | (-211) |
$2,751 49,531 kWh |
$(-707) (-211) MMBtu |
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05: 2.6212 TURN OFF EQUIPMENT DURING BREAKS, REDUCE OPERATING TIME |
Savings: $1,737 Cost: - |
$1,737 | 31,067 | - | - |
$1,737 31,067 kWh |
- - MMBtu |
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06: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $8,056 Cost: $500 |
- | - | $8,056 | 2,398 |
- - kWh |
$8,056 2,398 MMBtu |
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07: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT |
Savings: $18,343 Cost: $6,900 |
- | - | $18,343 | 5,459 |
- - kWh |
$18,343 5,459 MMBtu |
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TOTAL RECOMMENDED |
Savings: $45,809 Cost: $18,806 |
$20,117 | 361,372 | $25,692 | 7,646 | $20,117 361,372 kWh |
$25,692 7,646 MMBtu |
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TOTAL IMPLEMENTED |
Savings: $35,594 Cost: $18,806 |
$9,902 | 177,902 | $25,692 | 7,646 | $9,902 177,902 kWh |
$25,692 7,646 MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |