Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
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Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
69
matching recommendationsSIC | 286 | Industrial Organic Chemicals |
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Row Colors Legend |
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no implementation information |
Implemented |
NOT Implemented |
ID | # | Year | Products | Savings | Cost | Status |
---|---|---|---|---|---|---|
AM0628 # 06 Y:2013 | 06 | 2013 | INSTALL SKYLIGHTS | $1,525 | $0 | Implemented |
AM0628 # 07 Y:2013 | 07 | 2013 | INSULATE FEEDWATER TANK | $820 | $455 | Implemented |
AM0628 # 08 Y:2013 | 08 | 2013 | UTILIZE DAYLIGHT WHENEVER POSSIBLE IN LIEU OF ARTIFICIAL LIGHT | $520 | $0 | Implemented |
AM0628 # 09 Y:2013 | 09 | 2013 | USE SYNTHETIC LUBRICANT | $240 | $0 | Not Implemented |
OK0718 # 02 Y:2005 | 02 | 2005 | ELIMINATE OR REDUCE COMPRESSED AIR USAGE | $13,021 | $40,875 | Not Implemented |
OK0718 # 01 Y:2005 | 01 | 2005 | DEVELOP A REPAIR/REPLACE POLICY | $12,970 | $500 | Implemented |
OK0718 # 03 Y:2005 | 03 | 2005 | USE COMPRESSOR AIR FILTERS | $5,034 | $459 | Not Implemented |
OK0718 # 04 Y:2005 | 04 | 2005 | ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO | $4,239 | $8,030 | Not Implemented |
OK0718 # 05 Y:2005 | 05 | 2005 | PREHEAT BOILER MAKEUP WATER WITH WASTE PROCESS HEAT | $2,243 | $5,175 | Not Implemented |
OK0718 # 06 Y:2005 | 06 | 2005 | INSULATE BARE EQUIPMENT | $1,343 | $1,693 | Implemented |
OK0718 # 07 Y:2005 | 07 | 2005 | USE OPTIMUM THICKNESS INSULATION | $2,162 | $1,710 | Implemented |
OK0718 # 08 Y:2005 | 08 | 2005 | UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS | $14,226 | $66,500 | Implemented |
AM0402 # 01 Y:2001 | 01 | 2001 | REPAIR OR REPLACE STEAM TRAPS | $632,000 | $1,210 | Implemented |
AM0402 # 11 Y:2001 | 11 | 2001 | MAKE A PRACTICE OF TURNING OFF LIGHTS WHEN NOT NEEDED | $4,010 | $0 | Implemented |
AM0402 # 02 Y:2001 | 02 | 2001 | USE A FOSSIL FUEL ENGINE TO COGENERATE ELECTRICITY OR MOTIVE POWER; AND UTILIZE HEAT | $248,500 | $1,730,000 | Not Implemented |
AM0402 # 03 Y:2001 | 03 | 2001 | INCREASE AMOUNT OF CONDENSATE RETURNED | $61,175 | $15,000 | n/a |
AM0402 # 04 Y:2001 | 04 | 2001 | REPAIR AND ELIMINATE STEAM LEAKS | $27,400 | $1,000 | Implemented |
AM0402 # 05 Y:2001 | 05 | 2001 | USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM | $26,070 | $53,700 | n/a |
AM0402 # 06 Y:2001 | 06 | 2001 | INSULATE BARE EQUIPMENT | $19,300 | $865 | Implemented |
AM0402 # 07 Y:2001 | 07 | 2001 | USE SYNTHETIC LUBRICANT | $11,100 | $0 | Not Implemented |
AM0402 # 08 Y:2001 | 08 | 2001 | USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS | $10,700 | $3,300 | Not Implemented |
AM0402 # 09 Y:2001 | 09 | 2001 | TURN OFF EQUIPMENT DURING BREAKS, REDUCE OPERATING TIME | $8,200 | $0 | Implemented |
AM0402 # 10 Y:2001 | 10 | 2001 | RESCHEDULE PLANT OPERATIONS OR REDUCE LOAD TO AVOID PEAKS | $4,325 | $0 | Implemented |
AM0167 # 02 Y:1993 | 02 | 1993 | OPTIMIZE PLANT POWER FACTOR | $10,100 | $16,000 | Implemented |
AM0167 # 05 Y:1993 | 05 | 1993 | USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT INCOMING FLUIDS | $2,970 | $2,450 | Not Implemented |