Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Texas A&M, College Station |
---|---|
Assessment Year | 1990 |
Principal Product | FRESH MEAT AND SAUSAGES |
NAICS | n/a |
SIC | 2011 - Meat Packing Plants |
Sales | $10,000,000-$50,000,000 |
# of Employees | 75 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 25,000 Pieces |
Production Hrs. Annual | 5,300 |
Location (State) | TX |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $91,372 | 1,470,106 | kWh | $0.06 |
Natural Gas | $60,128 | 13,020 | MMBtu | $4.62 |
TOTAL ENERGY COSTS | $151,500 | |||
RECOMMENDED SAVINGS* | $3,400 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $449 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.2121 INCREASE AMOUNT OF CONDENSATE RETURNED |
Savings: $1,357 Cost: - |
- | - | $1,150 | 252 | $207 | - |
- - kWh |
$1,150 252 MMBtu |
$207 - $ |
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02: 2.3131 RESCHEDULE PLANT OPERATIONS OR REDUCE LOAD TO AVOID PEAKS |
Savings: $700 Cost: - |
$700 | - | - | - | - | - |
$700 - kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.8112 COMBINE UTILITY METERS |
Savings: $694 Cost: $1,100 |
- | - | $694 | - | - | - |
- - kWh |
$694 - MMBtu |
- - $ |
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04: 2.2511 INSULATE BARE EQUIPMENT |
Savings: $250 Cost: $60 |
- | - | $250 | 56 | - | - |
- - kWh |
$250 56 MMBtu |
- - $ |
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05: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $200 Cost: $530 |
- | - | $200 | 44 | - | - |
- - kWh |
$200 44 MMBtu |
- - $ |
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06: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $136 Cost: $52 |
$136 | 3,224 | - | - | - | - |
$136 3,224 kWh |
- - MMBtu |
- - $ |
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07: 2.7133 USE SEPARATE SWITCHES ON PERIMETER LIGHTING WHICH MAY BE TURNED OFF WHEN NATURAL LIGHT IS AVAILABLE |
Savings: $63 Cost: - |
$63 | 2,638 | - | - | - | - |
$63 2,638 kWh |
- - MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $3,400 Cost: $1,742 |
$899 | 5,862 | $2,294 | 352 | $207 | - | $899 5,862 kWh |
$2,294 352 MMBtu |
$207 - $ |
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TOTAL IMPLEMENTED |
Savings: $449 Cost: $112 |
$199 | 5,862 | $250 | 56 | - | - | $199 5,862 kWh |
$250 56 MMBtu |
- - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |