Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | North Carolina A&T |
---|---|
Assessment Year | 1986 |
Principal Product | RUBBER & PLASTIC HOSES |
NAICS | n/a |
SIC | 3069 - Fabricated Rubber Products, Nec |
Sales | $10,000,000-$50,000,000 |
# of Employees | 250 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 2,500 Thousand Feet |
Production Hrs. Annual | 6,468 |
Location (State) | NC |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $313,709 | 5,958,968 | kWh | $0.05 |
Natural Gas | $113,697 | 19,824 | MMBtu | $5.74 |
TOTAL ENERGY COSTS | $427,406 | |||
RECOMMENDED SAVINGS* | $21,994 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $21,994 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $2,704 Cost: $2,411 |
$2,704 | 51,290 | - | - |
$2,704 51,290 kWh |
- - MMBtu |
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02: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $439 Cost: $79 |
$439 | 8,206 | - | - |
$439 8,206 kWh |
- - MMBtu |
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03: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $4,902 Cost: $300 |
- | - | $4,902 | 854 |
- - kWh |
$4,902 854 MMBtu |
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04: 2.2121 INCREASE AMOUNT OF CONDENSATE RETURNED |
Savings: $3,940 Cost: $5,000 |
- | - | $3,940 | 686 |
- - kWh |
$3,940 686 MMBtu |
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05: 2.2614 USE COOLING TOWER OR ECONOMIZER TO REPLACE CHILLER COOLING |
Savings: $10,009 Cost: $2,000 |
$10,009 | 190,211 | - | - |
$10,009 190,211 kWh |
- - MMBtu |
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TOTAL RECOMMENDED |
Savings: $21,994 Cost: $9,790 |
$13,152 | 249,707 | $8,842 | 1,540 | $13,152 249,707 kWh |
$8,842 1,540 MMBtu |
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TOTAL IMPLEMENTED |
Savings: $21,994 Cost: $9,790 |
$13,152 | 249,707 | $8,842 | 1,540 | $13,152 249,707 kWh |
$8,842 1,540 MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |