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IAC Assessment: AT0107
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IAC Assessment: AT0107
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IAC Center North Carolina A&T
Assessment Year 1988
Principal Product MOLDED RUBBER PRODUCTS
NAICS n/a
SIC 3069 - Fabricated Rubber Products, Nec
Sales $10,000,000-$50,000,000
# of Employees 158
Plant Area (Sq.Ft.) 0
Annual Production 200,000 Pounds
Production Hrs. Annual 6,240
Location (State) VA
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $182,036 3,715,123 kWh $0.05
Natural Gas $155,797 36,677 MMBtu $4.25
TOTAL ENERGY COSTS $337,833
RECOMMENDED SAVINGS* $55,540 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $49,484
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.3131 RESCHEDULE PLANT OPERATIONS OR REDUCE LOAD TO AVOID PEAKS Savings:
$43,172
Cost:
-
$41,716 - - - $1,456 - $41,716
-
kWh
-
-
MMBtu
$1,456
-
$
02: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT Savings:
$5,252
Cost:
$8,000
- - $5,252 1,300 - - -
-
kWh
$5,252
1,300
MMBtu
-
-
$
03: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$406
Cost:
-
- - $906 224 $(-500) - -
-
kWh
$906
224
MMBtu
$(-500)
-
$
04: 2.2122 INSTALL / REPAIR INSULATION ON CONDENSATE LINES Savings:
$139
Cost:
-
- - $139 34 - - -
-
kWh
$139
34
MMBtu
-
-
$
05: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$531
Cost:
$490
$531 10,844 - - - - $531
10,844
kWh
-
-
MMBtu
-
-
$
06: 2.7221 LOWER TEMPERATURE DURING THE WINTER SEASON AND VICE-VERSA Savings:
$1,249
Cost:
$1,400
$1,249 25,498 - - - - $1,249
25,498
kWh
-
-
MMBtu
-
-
$
07: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$1,436
Cost:
-
$1,436 29,308 - - - - $1,436
29,308
kWh
-
-
MMBtu
-
-
$
08: 2.4221 INSTALL COMPRESSOR AIR INTAKES IN COOLEST LOCATIONS Savings:
$789
Cost:
$1,000
$789 16,120 - - - - $789
16,120
kWh
-
-
MMBtu
-
-
$
09: 2.4312 IMPROVE LUBRICATION PRACTICES Savings:
$586
Cost:
-
$586 12,016 - - - - $586
12,016
kWh
-
-
MMBtu
-
-
$
10: 2.2511 INSULATE BARE EQUIPMENT Savings:
$664
Cost:
$500
$664 48,066 - - - - $664
48,066
kWh
-
-
MMBtu
-
-
$
11: 2.7111 REDUCE ILLUMINATION TO MINIMUM NECESSARY LEVELS Savings:
$804
Cost:
$2,635
$804 16,413 - - - - $804
16,413
kWh
-
-
MMBtu
-
-
$
12: 2.7314 REDUCE VENTILATION AIR Savings:
$512
Cost:
$300
$512 10,551 - - - - $512
10,551
kWh
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$55,540
Cost:
$14,325
$48,287 168,816 $6,297 1,558 $956 - $48,287
168,816
kWh
$6,297
1,558
MMBtu
$956
-
$
TOTAL IMPLEMENTED Savings:
$49,484
Cost:
$3,690
$47,483 152,403 $1,045 258 $956 - $47,483
152,403
kWh
$1,045
258
MMBtu
$956
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes