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IAC Assessment: GT0211
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IAC Assessment: GT0211
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IAC Center Georgia Institute of Technology
Assessment Year 1984
Principal Product YARN DYEING
NAICS n/a
SIC 2269 - Finishing Plants, Nec
Sales $1,000,000-$5,000,000
# of Employees 50
Plant Area (Sq.Ft.) 0
Annual Production 3,000,000 Pounds
Production Hrs. Annual 4,896
Location (State) GA
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $33,343 703,986 kWh $0.05
Natural Gas $194,612 45,155 MMBtu $4.31
TOTAL ENERGY COSTS $227,955
RECOMMENDED SAVINGS* $93,648 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $93,648
#|Description Savings
Cost
Status Electricity Usage Natural Gas Coal Administrative Changes Electricity Usage Natural Gas Coal Administrative Changes
$ kWh $ MMBtu $ MMBtu $ $
01: 2.2449 RECOVER HEAT FROM EXHAUSTED STEAM, HOT AIR OR HOT WATER Savings:
$19,964
Cost:
$32,000
- - $19,964 4,765 - - - - -
-
kWh
$19,964
4,765
MMBtu
-
-
MMBtu
-
-
$
02: 2.2514 COVER OPEN TANKS Savings:
$2,894
Cost:
$4,000
- - $2,894 690 - - - - -
-
kWh
$2,894
690
MMBtu
-
-
MMBtu
-
-
$
03: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS Savings:
$300
Cost:
$50
- - $300 70 - - - - -
-
kWh
$300
70
MMBtu
-
-
MMBtu
-
-
$
04: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES Savings:
$985
Cost:
$432
- - $985 234 - - - - -
-
kWh
$985
234
MMBtu
-
-
MMBtu
-
-
$
05: 2.2122 INSTALL / REPAIR INSULATION ON CONDENSATE LINES Savings:
$335
Cost:
$148
- - $335 80 - - - - -
-
kWh
$335
80
MMBtu
-
-
MMBtu
-
-
$
06: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$808
Cost:
$104
$808 16,999 - - - - - - $808
16,999
kWh
-
-
MMBtu
-
-
MMBtu
-
-
$
07: 2.1331 BURN A LESS EXPENSIVE GRADE OF FUEL Savings:
$67,362
Cost:
$200,000
- - $194,612 46,500 $(-116,250) (-46,500) $(-11,000) - -
-
kWh
$194,612
46,500
MMBtu
$(-116,250)
(-46,500)
MMBtu
$(-11,000)
-
$
08: 2.2121 INCREASE AMOUNT OF CONDENSATE RETURNED Savings:
$1,000
Cost:
$8,000
- - $1,000 240 - - - - -
-
kWh
$1,000
240
MMBtu
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$93,648
Cost:
$244,734
$808 16,999 $220,090 52,579 $(-116,250) (-46,500) $(-11,000) - $808
16,999
kWh
$220,090
52,579
MMBtu
$(-116,250)
(-46,500)
MMBtu
$(-11,000)
-
$
TOTAL IMPLEMENTED Savings:
$93,648
Cost:
$244,734
$808 16,999 $220,090 52,579 $(-116,250) (-46,500) $(-11,000) - $808
16,999
kWh
$220,090
52,579
MMBtu
$(-116,250)
(-46,500)
MMBtu
$(-11,000)
-
$
Savings
Cost
$ kWh $ MMBtu $ MMBtu $ $
Electricity Usage Natural Gas Coal Administrative Changes Electricity Usage Natural Gas Coal Administrative Changes