Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
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Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Georgia Institute of Technology |
---|---|
Assessment Year | 1984 |
Principal Product | YARN DYEING |
NAICS | n/a |
SIC | 2269 - Finishing Plants, Nec |
Sales | $1,000,000-$5,000,000 |
# of Employees | 50 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 3,000,000 Pounds |
Production Hrs. Annual | 4,896 |
Location (State) | GA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $33,343 | 703,986 | kWh | $0.05 |
Natural Gas | $194,612 | 45,155 | MMBtu | $4.31 |
TOTAL ENERGY COSTS | $227,955 | |||
RECOMMENDED SAVINGS* | $93,648 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $93,648 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Coal | Administrative Changes | Electricity Usage | Natural Gas | Coal | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.2449 RECOVER HEAT FROM EXHAUSTED STEAM, HOT AIR OR HOT WATER |
Savings: $19,964 Cost: $32,000 |
- | - | $19,964 | 4,765 | - | - | - | - |
- - kWh |
$19,964 4,765 MMBtu |
- - MMBtu |
- - $ |
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02: 2.2514 COVER OPEN TANKS |
Savings: $2,894 Cost: $4,000 |
- | - | $2,894 | 690 | - | - | - | - |
- - kWh |
$2,894 690 MMBtu |
- - MMBtu |
- - $ |
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03: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $300 Cost: $50 |
- | - | $300 | 70 | - | - | - | - |
- - kWh |
$300 70 MMBtu |
- - MMBtu |
- - $ |
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04: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $985 Cost: $432 |
- | - | $985 | 234 | - | - | - | - |
- - kWh |
$985 234 MMBtu |
- - MMBtu |
- - $ |
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05: 2.2122 INSTALL / REPAIR INSULATION ON CONDENSATE LINES |
Savings: $335 Cost: $148 |
- | - | $335 | 80 | - | - | - | - |
- - kWh |
$335 80 MMBtu |
- - MMBtu |
- - $ |
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06: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $808 Cost: $104 |
$808 | 16,999 | - | - | - | - | - | - |
$808 16,999 kWh |
- - MMBtu |
- - MMBtu |
- - $ |
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07: 2.1331 BURN A LESS EXPENSIVE GRADE OF FUEL |
Savings: $67,362 Cost: $200,000 |
- | - | $194,612 | 46,500 | $(-116,250) | (-46,500) | $(-11,000) | - |
- - kWh |
$194,612 46,500 MMBtu |
$(-116,250) (-46,500) MMBtu |
$(-11,000) - $ |
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08: 2.2121 INCREASE AMOUNT OF CONDENSATE RETURNED |
Savings: $1,000 Cost: $8,000 |
- | - | $1,000 | 240 | - | - | - | - |
- - kWh |
$1,000 240 MMBtu |
- - MMBtu |
- - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $93,648 Cost: $244,734 |
$808 | 16,999 | $220,090 | 52,579 | $(-116,250) | (-46,500) | $(-11,000) | - | $808 16,999 kWh |
$220,090 52,579 MMBtu |
$(-116,250) (-46,500) MMBtu |
$(-11,000) - $ |
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TOTAL IMPLEMENTED |
Savings: $93,648 Cost: $244,734 |
$808 | 16,999 | $220,090 | 52,579 | $(-116,250) | (-46,500) | $(-11,000) | - | $808 16,999 kWh |
$220,090 52,579 MMBtu |
$(-116,250) (-46,500) MMBtu |
$(-11,000) - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Coal | Administrative Changes | Electricity Usage | Natural Gas | Coal | Administrative Changes |