Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Georgia Institute of Technology |
---|---|
Assessment Year | 1984 |
Principal Product | DYED & FINISHED PRODUCTS |
NAICS | n/a |
SIC | 2262 - Finishing Plants, Manmade |
Sales | $10,000,000-$50,000,000 |
# of Employees | 200 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 144,000 Thousand Feet |
Production Hrs. Annual | 7,344 |
Location (State) | GA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $273,352 | 5,790,446 | kWh | $0.05 |
Natural Gas | $797,195 | 191,447 | MMBtu | $4.16 |
Fuel Oil #6 | $50,752 | 10,493 | MMBtu | $4.84 |
TOTAL ENERGY COSTS | $1,121,299 | |||
RECOMMENDED SAVINGS* | $297,447 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | $53,717 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $20,387 Cost: $200 |
- | - | $20,387 | 4,890 |
- - kWh |
$20,387 4,890 MMBtu |
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02: 2.1243 USE HEAT FROM BOILER BLOWDOWN TO PREHEAT BOILER FEED WATER |
Savings: $11,700 Cost: $10,000 |
- | - | $11,700 | 2,800 |
- - kWh |
$11,700 2,800 MMBtu |
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03: 2.2449 RECOVER HEAT FROM EXHAUSTED STEAM, HOT AIR OR HOT WATER |
Savings: $188,200 Cost: $270,000 |
- | - | $188,200 | 45,100 |
- - kWh |
$188,200 45,100 MMBtu |
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04: 2.5192 MODIFY TEXTILE DRYERS |
Savings: $51,600 Cost: $23,000 |
- | - | $51,600 | 12,375 |
- - kWh |
$51,600 12,375 MMBtu |
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05: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $19,960 Cost: $1,000 |
- | - | $19,960 | 4,770 |
- - kWh |
$19,960 4,770 MMBtu |
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06: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $1,670 Cost: $640 |
- | - | $1,670 | 400 |
- - kWh |
$1,670 400 MMBtu |
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07: 2.2122 INSTALL / REPAIR INSULATION ON CONDENSATE LINES |
Savings: $1,040 Cost: $400 |
- | - | $1,040 | 250 |
- - kWh |
$1,040 250 MMBtu |
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08: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $2,890 Cost: $2,520 |
$2,890 | 61,547 | - | - |
$2,890 61,547 kWh |
- - MMBtu |
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TOTAL RECOMMENDED |
Savings: $297,447 Cost: $307,760 |
$2,890 | 61,547 | $294,557 | 70,585 | $2,890 61,547 kWh |
$294,557 70,585 MMBtu |
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TOTAL IMPLEMENTED |
Savings: $53,717 Cost: $11,840 |
- | - | $53,717 | 12,860 | - - kWh |
$53,717 12,860 MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |