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IAC Assessment: LL0213
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IAC Assessment: LL0213
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IAC Center University of Louisiana, Lafayette
Assessment Year 2004
Principal Product oil and gas production
NAICS 211111 - Crude Petroleum and Natural Gas Extraction
SIC 1311 - Crude Petroleum And Natural Gas
Sales $100,000,000-$500,000,000
# of Employees 150
Plant Area (Sq.Ft.) 85,000
Annual Production 21,900,000 BBL
Production Hrs. Annual 8,760
Location (State) LA
Source Yearly Cost Usage Unit Unit Cost
Natural Gas $2,000,000 1,002,103 MMBtu $2.00
TOTAL ENERGY COSTS $2,000,000
RECOMMENDED SAVINGS* $677,100 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $570,749
#|Description Savings
Cost
Status Natural Gas Personnel Changes One-time Revenue or Avoided Cost Natural Gas Personnel Changes One-time Revenue or Avoided Cost
$ MMBtu $ $ $ $
01: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT Savings:
$479,962
Cost:
$1,400,000
$479,962 239,981 - - - - $479,962
239,981
MMBtu
-
-
$
-
-
$
02: 2.1336 INSTALL EQUIPMENT TO UTILIZE WASTE FUEL Savings:
$55,846
Cost:
$100,000
$55,846 27,923 - - - - $55,846
27,923
MMBtu
-
-
$
-
-
$
03: 2.2693 USE WASTE HEAT STEAM FOR ABSORPTION REFRIGERATION Savings:
$47,454
Cost:
$108,000
$47,454 23,727 - - - - $47,454
23,727
MMBtu
-
-
$
-
-
$
04: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$11,231
Cost:
$4,806
$5,606 2,803 $5,625 - - - $5,606
2,803
MMBtu
$5,625
-
$
-
-
$
05: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$6,028
Cost:
$1,485
$6,028 3,014 - - - - $6,028
3,014
MMBtu
-
-
$
-
-
$
06: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$4,862
Cost:
$6,160
$4,862 2,431 - - - - $4,862
2,431
MMBtu
-
-
$
-
-
$
07: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$3,051
Cost:
$2,550
$684 352 $2,367 - - - $684
352
MMBtu
$2,367
-
$
-
-
$
08: 2.2511 INSULATE BARE EQUIPMENT Savings:
$1,146
Cost:
$492
$1,146 573 - - - - $1,146
573
MMBtu
-
-
$
-
-
$
09: 4.6110 BEGIN A PRACTICE OF PREDICTIVE / PREVENTATIVE MAINTENANCE Savings:
$67,520
Cost:
$4,000
- - $64,020 - $3,500 - -
-
MMBtu
$64,020
-
$
$3,500
-
$
TOTAL RECOMMENDED Savings:
$677,100
Cost:
$1,627,493
$601,588 300,804 $72,012 - $3,500 - $601,588
300,804
MMBtu
$72,012
-
$
$3,500
-
$
TOTAL IMPLEMENTED Savings:
$570,749
Cost:
$1,416,943
$497,604 248,802 $69,645 - $3,500 - $497,604
248,802
MMBtu
$69,645
-
$
$3,500
-
$
Savings
Cost
$ MMBtu $ $ $ $
Natural Gas Personnel Changes One-time Revenue or Avoided Cost Natural Gas Personnel Changes One-time Revenue or Avoided Cost