IAC logo
IAC Assessment: LL0213
Sponsored by:
DOE MESC
IAC logo
IAC Assessment: LL0213
Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center University of Louisiana, Lafayette
Assessment Year 2004
Principal Product oil and gas production
NAICS 211111 - Crude Petroleum and Natural Gas Extraction
SIC 1311 - Crude Petroleum And Natural Gas
Sales $100,000,000-$500,000,000
# of Employees 150
Plant Area (Sq.Ft.) 85,000
Annual Production 21,900,000 BBL
Production Hrs. Annual 8,760
Location (State) LA
Source Yearly Cost Usage Unit Unit Cost
Natural Gas $2,000,000 1,002,103 MMBtu $2.00
TOTAL ENERGY COSTS $2,000,000
RECOMMENDED SAVINGS* $677,100 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $570,749
#|Description Savings
Cost
Status Natural Gas Personnel Changes One-time Revenue or Avoided Cost Natural Gas Personnel Changes One-time Revenue or Avoided Cost
$ MMBtu $ $ $ $
01: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT Savings:
$479,962
Cost:
$1,400,000
$479,962 239,981 - - - - $479,962
239,981
MMBtu
-
-
$
-
-
$
02: 2.1336 INSTALL EQUIPMENT TO UTILIZE WASTE FUEL Savings:
$55,846
Cost:
$100,000
$55,846 27,923 - - - - $55,846
27,923
MMBtu
-
-
$
-
-
$
03: 2.2693 USE WASTE HEAT STEAM FOR ABSORPTION REFRIGERATION Savings:
$47,454
Cost:
$108,000
$47,454 23,727 - - - - $47,454
23,727
MMBtu
-
-
$
-
-
$
04: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$11,231
Cost:
$4,806
$5,606 2,803 $5,625 - - - $5,606
2,803
MMBtu
$5,625
-
$
-
-
$
05: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$6,028
Cost:
$1,485
$6,028 3,014 - - - - $6,028
3,014
MMBtu
-
-
$
-
-
$
06: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$4,862
Cost:
$6,160
$4,862 2,431 - - - - $4,862
2,431
MMBtu
-
-
$
-
-
$
07: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$3,051
Cost:
$2,550
$684 352 $2,367 - - - $684
352
MMBtu
$2,367
-
$
-
-
$
08: 2.2511 INSULATE BARE EQUIPMENT Savings:
$1,146
Cost:
$492
$1,146 573 - - - - $1,146
573
MMBtu
-
-
$
-
-
$
09: 4.611 BEGIN A PRACTICE OF PREDICTIVE / PREVENTATIVE MAINTENANCE Savings:
$67,520
Cost:
$4,000
- - $64,020 - $3,500 - -
-
MMBtu
$64,020
-
$
$3,500
-
$
TOTAL RECOMMENDED Savings:
$677,100
Cost:
$1,627,493
$601,588 300,804 $72,012 - $3,500 - $601,588
300,804
MMBtu
$72,012
-
$
$3,500
-
$
TOTAL IMPLEMENTED Savings:
$570,749
Cost:
$1,416,943
$497,604 248,802 $69,645 - $3,500 - $497,604
248,802
MMBtu
$69,645
-
$
$3,500
-
$
Savings
Cost
$ MMBtu $ $ $ $
Natural Gas Personnel Changes One-time Revenue or Avoided Cost Natural Gas Personnel Changes One-time Revenue or Avoided Cost