Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Notre Dame Univ. |
---|---|
Assessment Year | 1993 |
Principal Product | Forged Products |
NAICS | n/a |
SIC | 3462 - Iron And Steel Forgings |
Sales | $10,000,000-$50,000,000 |
# of Employees | 345 |
Plant Area (Sq.Ft.) | 215,000 |
Annual Production | 28,856 Pieces |
Production Hrs. Annual | 5,000 |
Location (State) | IN |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $807,605 | 12,185,229 | kWh | $0.07 |
Natural Gas | $920,565 | 356,270 | MMBtu | $2.58 |
TOTAL ENERGY COSTS | $1,728,170 | |||
RECOMMENDED SAVINGS* | $95,826 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $34,400 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.3411 REPLACE ELECTRIC MOTORS WITH BACK PRESSURE STEAM TURBINES AND USE EXHAUST STEAM FOR PROCESS HEAT |
Savings: $48,899 Cost: - |
$48,899 | 737,984 | - | - |
$48,899 737,984 kWh |
- - MMBtu |
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02: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $6,413 Cost: $6,235 |
$6,413 | 97,011 | - | - |
$6,413 97,011 kWh |
- - MMBtu |
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03: 2.8122 USE UTILITY CONTROLLED POWER MANAGEMENT |
Savings: $12,899 Cost: - |
$12,899 | 194,607 | - | - |
$12,899 194,607 kWh |
- - MMBtu |
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04: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $12,527 Cost: $1,413 |
$12,527 | 189,039 | - | - |
$12,527 189,039 kWh |
- - MMBtu |
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05: 2.3212 OPTIMIZE PLANT POWER FACTOR |
Savings: $11,871 Cost: $16,760 |
$11,871 | - | - | - |
$11,871 - kWh |
- - MMBtu |
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06: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $2,992 Cost: $1,262 |
$2,992 | 45,135 | - | - |
$2,992 45,135 kWh |
- - MMBtu |
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07: 2.2122 INSTALL / REPAIR INSULATION ON CONDENSATE LINES |
Savings: $225 Cost: $218 |
- | - | $225 | 87 |
- - kWh |
$225 87 MMBtu |
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TOTAL RECOMMENDED |
Savings: $95,826 Cost: $25,888 |
$95,601 | 1,263,776 | $225 | 87 | $95,601 1,263,776 kWh |
$225 87 MMBtu |
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TOTAL IMPLEMENTED |
Savings: $34,400 Cost: $24,475 |
$34,175 | 336,753 | $225 | 87 | $34,175 336,753 kWh |
$225 87 MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |