Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Oklahoma State University |
---|---|
Assessment Year | 1993 |
Principal Product | Tubular Goods |
NAICS | n/a |
SIC | 3533 - Oil And Gas Field Machinery |
Sales | $10,000,000-$50,000,000 |
# of Employees | 98 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 44,607 Tons |
Production Hrs. Annual | 3,432 |
Location (State) | OK |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $359,829 | 6,069,461 | kWh | $0.06 |
Natural Gas | $444,829 | 168,042 | MMBtu | $2.65 |
TOTAL ENERGY COSTS | $804,658 | |||
RECOMMENDED SAVINGS* | $65,281 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | $13,517 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $10,868 Cost: - |
$10,868 | 367,526 | - | - |
$10,868 367,526 kWh |
- - MMBtu |
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02: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $6,357 Cost: $4,918 |
$6,357 | 121,043 | - | - |
$6,357 121,043 kWh |
- - MMBtu |
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03: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $4,487 Cost: $11,785 |
$4,487 | 79,719 | - | - |
$4,487 79,719 kWh |
- - MMBtu |
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04: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $1,725 Cost: $3,693 |
$1,725 | 37,808 | - | - |
$1,725 37,808 kWh |
- - MMBtu |
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05: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $948 Cost: $1,079 |
$948 | 20,809 | - | - |
$948 20,809 kWh |
- - MMBtu |
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06: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $612 Cost: $749 |
$612 | 10,844 | - | - |
$612 10,844 kWh |
- - MMBtu |
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07: 2.1116 IMPROVE COMBUSTION CONTROL CAPABILITY |
Savings: $40,284 Cost: $190,000 |
- | - | $40,284 | 15,218 |
- - kWh |
$40,284 15,218 MMBtu |
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TOTAL RECOMMENDED |
Savings: $65,281 Cost: $212,224 |
$24,997 | 637,749 | $40,284 | 15,218 | $24,997 637,749 kWh |
$40,284 15,218 MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: $13,517 Cost: $21,475 |
$13,517 | 259,379 | - | - | $13,517 259,379 kWh |
- - MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |