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IAC Assessment: OR0130
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IAC Assessment: OR0130
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IAC Center Oregon State University
Assessment Year 1991
Principal Product BEEF AND PORK PRODUCTS
NAICS n/a
SIC 2011 - Meat Packing Plants
Sales $10,000,000-$50,000,000
# of Employees 85
Plant Area (Sq.Ft.) 0
Annual Production 20,000,000 Pounds
Production Hrs. Annual 8,736
Location (State) OR
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $97,777 2,307,444 kWh $0.04
Natural Gas $61,978 16,037 MMBtu $3.86
LPG $4,935 645 MMBtu $7.65
TOTAL ENERGY COSTS $164,690
RECOMMENDED SAVINGS* $10,249 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $10,249
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.6232 INSTALL SET-BACK TIMERS Savings:
$1,778
Cost:
$225
$1,778 35,756 - - - - $1,778
35,756
kWh
-
-
MMBtu
-
-
$
02: 3.4154 ELIMINATE LEAKS IN WATER LINES AND VALVES Savings:
$261
Cost:
-
- - $208 56 $53 - -
-
kWh
$208
56
MMBtu
$53
-
$
03: 2.2122 INSTALL / REPAIR INSULATION ON CONDENSATE LINES Savings:
$450
Cost:
$800
- - $450 120 - - -
-
kWh
$450
120
MMBtu
-
-
$
04: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$2,399
Cost:
$4,936
$2,399 57,444 - - - - $2,399
57,444
kWh
-
-
MMBtu
-
-
$
05: 2.3212 OPTIMIZE PLANT POWER FACTOR Savings:
$1,647
Cost:
$3,450
$1,647 - - - - - $1,647
-
kWh
-
-
MMBtu
-
-
$
06: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$75
Cost:
$157
$75 1,758 - - - - $75
1,758
kWh
-
-
MMBtu
-
-
$
07: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT Savings:
$3,347
Cost:
$3,453
- - $3,347 901 - - -
-
kWh
$3,347
901
MMBtu
-
-
$
08: 2.2122 INSTALL / REPAIR INSULATION ON CONDENSATE LINES Savings:
$292
Cost:
$881
- - $292 77 - - -
-
kWh
$292
77
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$10,249
Cost:
$13,902
$5,899 94,958 $4,297 1,154 $53 - $5,899
94,958
kWh
$4,297
1,154
MMBtu
$53
-
$
TOTAL IMPLEMENTED Savings:
$10,249
Cost:
$13,902
$5,899 94,958 $4,297 1,154 $53 - $5,899
94,958
kWh
$4,297
1,154
MMBtu
$53
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes