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IAC Assessment: OR0143
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IAC Assessment: OR0143
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IAC Center Oregon State University
Assessment Year 1992
Principal Product MARGARINE,SHORTENING,ETC
NAICS n/a
SIC 2079 - Edible Fats And Oils, Nec
Sales $10,000,000-$50,000,000
# of Employees 75
Plant Area (Sq.Ft.) 0
Annual Production 81,000,000 Pounds
Production Hrs. Annual 3,120
Location (State) OR
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $66,024 1,848,769 kWh $0.04
Natural Gas $41,495 12,538 MMBtu $3.31
TOTAL ENERGY COSTS $107,519
RECOMMENDED SAVINGS* $11,518 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $10,914
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.6232 INSTALL SET-BACK TIMERS Savings:
$4,147
Cost:
-
$2,970 114,009 - - $1,177 - $2,970
114,009
kWh
-
-
MMBtu
$1,177
-
$
02: 2.2621 MODIFY REFRIGERATION SYSTEM TO OPERATE AT A LOWER PRESSURE Savings:
$522
Cost:
-
$522 19,930 - - - - $522
19,930
kWh
-
-
MMBtu
-
-
$
03: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$389
Cost:
-
$389 7,327 - - - - $389
7,327
kWh
-
-
MMBtu
-
-
$
04: 2.3212 OPTIMIZE PLANT POWER FACTOR Savings:
$1,627
Cost:
$200
$1,627 - - - - - $1,627
-
kWh
-
-
MMBtu
-
-
$
05: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$1,840
Cost:
$1,000
- - $1,840 556 - - -
-
kWh
$1,840
556
MMBtu
-
-
$
06: 2.2121 INCREASE AMOUNT OF CONDENSATE RETURNED Savings:
$2,767
Cost:
$1,955
- - $2,509 758 $258 - -
-
kWh
$2,509
758
MMBtu
$258
-
$
07: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$144
Cost:
$2,216
$144 4,103 - - - - $144
4,103
kWh
-
-
MMBtu
-
-
$
08: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$82
Cost:
$514
$105 2,638 - - $(-23) - $105
2,638
kWh
-
-
MMBtu
$(-23)
-
$
TOTAL RECOMMENDED Savings:
$11,518
Cost:
$5,885
$5,757 148,007 $4,349 1,314 $1,412 - $5,757
148,007
kWh
$4,349
1,314
MMBtu
$1,412
-
$
TOTAL IMPLEMENTED Savings:
$10,914
Cost:
$5,371
$5,130 125,439 $4,349 1,314 $1,435 - $5,130
125,439
kWh
$4,349
1,314
MMBtu
$1,435
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes