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IAC Assessment: RU0143
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IAC Assessment: RU0143
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IAC Center Rutgers, State Univ. of NJ
Assessment Year 1992
Principal Product DIE CAST MOLDS
NAICS n/a
SIC 3544 - Special Dies, Tools, Jigs & Fixtures
Sales $10,000,000-$50,000,000
# of Employees 160
Plant Area (Sq.Ft.) 0
Annual Production 7,000 Pieces
Production Hrs. Annual 6,240
Location (State) NJ
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $250,612 2,654,455 kWh $0.09
Natural Gas $18,053 2,690 MMBtu $6.71
TOTAL ENERGY COSTS $268,665
RECOMMENDED SAVINGS* $31,125 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $5,214
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$3,359
Cost:
$5,963
$4,342 46,014 - - $(-983) - $4,342
46,014
kWh
-
-
MMBtu
$(-983)
-
$
02: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$650
Cost:
$500
- - $650 97 - - -
-
kWh
$650
97
MMBtu
-
-
$
03: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES Savings:
$1,855
Cost:
$930
- - $1,855 277 - - -
-
kWh
$1,855
277
MMBtu
-
-
$
04: 2.7494 INSTALL STORM WINDOWS AND DOORS Savings:
$508
Cost:
$1,100
- - $508 76 - - -
-
kWh
$508
76
MMBtu
-
-
$
05: 2.3191 USE DEMAND CONTROLLER OR LOAD SHEDDER Savings:
$6,177
Cost:
$2,500
$6,177 - - - - - $6,177
-
kWh
-
-
MMBtu
-
-
$
06: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$4,275
Cost:
$2,098
$4,275 45,428 - - - - $4,275
45,428
kWh
-
-
MMBtu
-
-
$
07: 2.4312 IMPROVE LUBRICATION PRACTICES Savings:
$10,595
Cost:
$800
$10,595 112,837 - - - - $10,595
112,837
kWh
-
-
MMBtu
-
-
$
08: 2.8114 CHANGE RATE SCHEDULES OR OTHER CHANGES IN UTILITY SERVICE Savings:
$3,706
Cost:
$4,000
$3,706 - - - - - $3,706
-
kWh
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$31,125
Cost:
$17,891
$29,095 204,279 $3,013 450 $(-983) - $29,095
204,279
kWh
$3,013
450
MMBtu
$(-983)
-
$
TOTAL IMPLEMENTED Savings:
$5,214
Cost:
$6,893
$4,342 46,014 $1,855 277 $(-983) - $4,342
46,014
kWh
$1,855
277
MMBtu
$(-983)
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes