IAC logo
IAC Assessment: RU0146
Sponsored by:
DOE MESC
IAC logo
IAC Assessment: RU0146
Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center Rutgers, State Univ. of NJ
Assessment Year 1992
Principal Product LABORATORY INSTRUMENTS
NAICS n/a
SIC 3821 - Laboratory Apparatus And Furniture
Sales $10,000,000-$50,000,000
# of Employees 128
Plant Area (Sq.Ft.) 0
Annual Production 3,500 Pieces
Production Hrs. Annual 2,600
Location (State) NJ
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $93,954 735,639 kWh $0.13
Natural Gas $12,810 2,126 MMBtu $6.03
TOTAL ENERGY COSTS $106,764
RECOMMENDED SAVINGS* $14,083 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* -
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$621
Cost:
$79
$936 14,654 - - $(-315) - $936
14,654
kWh
-
-
MMBtu
$(-315)
-
$
02: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$256
Cost:
$500
- - $256 43 - - -
-
kWh
$256
43
MMBtu
-
-
$
03: 2.7243 IMPROVE AIR CIRCULATION WITH DESTRATIFICATION FANS / OTHER METHODS Savings:
$1,643
Cost:
$3,420
$(-227) (-1,758) $1,870 312 - - $(-227)
(-1,758)
kWh
$1,870
312
MMBtu
-
-
$
04: 2.6232 INSTALL SET-BACK TIMERS Savings:
$3,358
Cost:
$956
$3,358 26,377 - - - - $3,358
26,377
kWh
-
-
MMBtu
-
-
$
05: 2.3191 USE DEMAND CONTROLLER OR LOAD SHEDDER Savings:
$4,489
Cost:
$2,500
$4,489 - - - - - $4,489
-
kWh
-
-
MMBtu
-
-
$
06: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$652
Cost:
$734
$652 4,982 - - - - $652
4,982
kWh
-
-
MMBtu
-
-
$
07: 2.4312 IMPROVE LUBRICATION PRACTICES Savings:
$1,624
Cost:
$800
$1,624 12,603 - - - - $1,624
12,603
kWh
-
-
MMBtu
-
-
$
08: 3.7214 REDUCE OR ELIMINATE WASTE Savings:
$1,440
Cost:
$450
- - - - $1,440 - -
-
kWh
-
-
MMBtu
$1,440
-
$
TOTAL RECOMMENDED Savings:
$14,083
Cost:
$9,439
$10,832 56,858 $2,126 355 $1,125 - $10,832
56,858
kWh
$2,126
355
MMBtu
$1,125
-
$
TOTAL IMPLEMENTED Savings:
-
Cost:
-
- - - - - - -
-
kWh
-
-
MMBtu
-
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes