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IAC Assessment: WI0007
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IAC Assessment: WI0007
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IAC Center University of Wisconsin, Milwaukee
Assessment Year 1987
Principal Product WATER SOFTENER CONTROLS
NAICS n/a
SIC 3491 - Industrial Valves
Sales $10,000,000-$50,000,000
# of Employees 125
Plant Area (Sq.Ft.) 0
Annual Production 150,000 Pieces
Production Hrs. Annual 2,125
Location (State) WI
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $64,599 945,780 kWh $0.07
Natural Gas $17,572 3,317 MMBtu $5.30
TOTAL ENERGY COSTS $82,171
RECOMMENDED SAVINGS* $3,539 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $2,905
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.4312 IMPROVE LUBRICATION PRACTICES Savings:
$330
Cost:
-
$330 4,982 - - - - $330
4,982
kWh
-
-
MMBtu
-
-
$
02: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$112
Cost:
-
$112 1,758 - - - - $112
1,758
kWh
-
-
MMBtu
-
-
$
03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$1,549
Cost:
$5,631
$1,549 22,567 - - - - $1,549
22,567
kWh
-
-
MMBtu
-
-
$
04: 2.6121 REDUCE HOT WATER TEMPERATURE TO THE MINIMUM REQUIRED Savings:
$129
Cost:
-
- - $129 24 - - -
-
kWh
$129
24
MMBtu
-
-
$
05: 2.3131 RESCHEDULE PLANT OPERATIONS OR REDUCE LOAD TO AVOID PEAKS Savings:
$634
Cost:
-
$634 - - - - - $634
-
kWh
-
-
MMBtu
-
-
$
06: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$387
Cost:
-
- - $387 73 - - -
-
kWh
$387
73
MMBtu
-
-
$
07: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$398
Cost:
$500
- - $498 94 $(-100) - -
-
kWh
$498
94
MMBtu
$(-100)
-
$
TOTAL RECOMMENDED Savings:
$3,539
Cost:
$6,131
$2,625 29,307 $1,014 191 $(-100) - $2,625
29,307
kWh
$1,014
191
MMBtu
$(-100)
-
$
TOTAL IMPLEMENTED Savings:
$2,905
Cost:
$6,131
$1,991 29,307 $1,014 191 $(-100) - $1,991
29,307
kWh
$1,014
191
MMBtu
$(-100)
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes