Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Wisconsin, Milwaukee |
---|---|
Assessment Year | 1987 |
Principal Product | WATER SOFTENER CONTROLS |
NAICS | n/a |
SIC | 3491 - Industrial Valves |
Sales | $10,000,000-$50,000,000 |
# of Employees | 125 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 150,000 Pieces |
Production Hrs. Annual | 2,125 |
Location (State) | WI |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $64,599 | 945,780 | kWh | $0.07 |
Natural Gas | $17,572 | 3,317 | MMBtu | $5.30 |
TOTAL ENERGY COSTS | $82,171 | |||
RECOMMENDED SAVINGS* | $3,539 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $2,905 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.4312 IMPROVE LUBRICATION PRACTICES |
Savings: $330 Cost: - |
$330 | 4,982 | - | - | - | - |
$330 4,982 kWh |
- - MMBtu |
- - $ |
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02: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $112 Cost: - |
$112 | 1,758 | - | - | - | - |
$112 1,758 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $1,549 Cost: $5,631 |
$1,549 | 22,567 | - | - | - | - |
$1,549 22,567 kWh |
- - MMBtu |
- - $ |
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04: 2.6121 REDUCE HOT WATER TEMPERATURE TO THE MINIMUM REQUIRED |
Savings: $129 Cost: - |
- | - | $129 | 24 | - | - |
- - kWh |
$129 24 MMBtu |
- - $ |
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05: 2.3131 RESCHEDULE PLANT OPERATIONS OR REDUCE LOAD TO AVOID PEAKS |
Savings: $634 Cost: - |
$634 | - | - | - | - | - |
$634 - kWh |
- - MMBtu |
- - $ |
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06: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $387 Cost: - |
- | - | $387 | 73 | - | - |
- - kWh |
$387 73 MMBtu |
- - $ |
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07: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $398 Cost: $500 |
- | - | $498 | 94 | $(-100) | - |
- - kWh |
$498 94 MMBtu |
$(-100) - $ |
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TOTAL RECOMMENDED |
Savings: $3,539 Cost: $6,131 |
$2,625 | 29,307 | $1,014 | 191 | $(-100) | - | $2,625 29,307 kWh |
$1,014 191 MMBtu |
$(-100) - $ |
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TOTAL IMPLEMENTED |
Savings: $2,905 Cost: $6,131 |
$1,991 | 29,307 | $1,014 | 191 | $(-100) | - | $1,991 29,307 kWh |
$1,014 191 MMBtu |
$(-100) - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |