IAC logo
IAC Assessment: WI0037
Sponsored by:
DOE MESC
IAC logo
IAC Assessment: WI0037
Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center University of Wisconsin, Milwaukee
Assessment Year 1988
Principal Product PISTONS, MOTORS, PUMPS
NAICS n/a
SIC 3594 - Fluid Power Pumps And Motors
Sales $10,000,000-$50,000,000
# of Employees 180
Plant Area (Sq.Ft.) 0
Annual Production 140,000 Pieces
Production Hrs. Annual 4,950
Location (State) IL
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $208,522 2,775,791 kWh $0.08
Natural Gas $41,865 12,827 MMBtu $3.26
TOTAL ENERGY COSTS $250,387
RECOMMENDED SAVINGS* $58,030 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $53,783
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.4312 IMPROVE LUBRICATION PRACTICES Savings:
$3,862
Cost:
-
$3,862 51,290 - - - - $3,862
51,290
kWh
-
-
MMBtu
-
-
$
02: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$1,535
Cost:
-
$1,535 20,516 - - - - $1,535
20,516
kWh
-
-
MMBtu
-
-
$
03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$43,747
Cost:
$33,748
$43,747 582,356 - - - - $43,747
582,356
kWh
-
-
MMBtu
-
-
$
04: 2.1311 REPLACE ELECTRICALLY-OPERATED EQUIPMENT WITH FOSSIL FUEL EQUIPMENT Savings:
$885
Cost:
$1,000
$1,086 14,361 $(-201) (-62) - - $1,086
14,361
kWh
$(-201)
(-62)
MMBtu
-
-
$
05: 2.3131 RESCHEDULE PLANT OPERATIONS OR REDUCE LOAD TO AVOID PEAKS Savings:
$3,732
Cost:
-
$3,732 - - - - - $3,732
-
kWh
-
-
MMBtu
-
-
$
06: 2.3132 RECHARGE BATTERIES ON DURING OFF-PEAK DEMAND PERIODS Savings:
$1,189
Cost:
-
$1,189 - - - - - $1,189
-
kWh
-
-
MMBtu
-
-
$
07: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT Savings:
$2,695
Cost:
$1,500
- - $2,695 827 - - -
-
kWh
$2,695
827
MMBtu
-
-
$
08: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$385
Cost:
$500
- - $685 210 $(-300) - -
-
kWh
$685
210
MMBtu
$(-300)
-
$
TOTAL RECOMMENDED Savings:
$58,030
Cost:
$36,748
$55,151 668,523 $3,179 975 $(-300) - $55,151
668,523
kWh
$3,179
975
MMBtu
$(-300)
-
$
TOTAL IMPLEMENTED Savings:
$53,783
Cost:
$36,248
$51,289 617,233 $2,494 765 - - $51,289
617,233
kWh
$2,494
765
MMBtu
-
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes