Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Wisconsin, Milwaukee |
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Assessment Year | 1988 |
Principal Product | RELAYS, SOLENOIDS |
NAICS | n/a |
SIC | 3679 - Electronic Components, Nec |
Sales | $10,000,000-$50,000,000 |
# of Employees | 260 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 3,800,000 Pieces |
Production Hrs. Annual | 6,000 |
Location (State) | WI |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $186,258 | 3,769,930 | kWh | $0.05 |
Natural Gas | $32,993 | 6,974 | MMBtu | $4.73 |
TOTAL ENERGY COSTS | $219,251 | |||
RECOMMENDED SAVINGS* | $13,009 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $4,082 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.4312 IMPROVE LUBRICATION PRACTICES |
Savings: $5,488 Cost: - |
$5,488 | 111,079 | - | - |
$5,488 111,079 kWh |
- - MMBtu |
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02: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $624 Cost: - |
$624 | 12,603 | - | - |
$624 12,603 kWh |
- - MMBtu |
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03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $1,829 Cost: $309 |
$1,829 | 36,928 | - | - |
$1,829 36,928 kWh |
- - MMBtu |
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04: 2.1311 REPLACE ELECTRICALLY-OPERATED EQUIPMENT WITH FOSSIL FUEL EQUIPMENT |
Savings: $1,254 Cost: $1,650 |
$2,114 | 42,790 | $(-860) | (-182) |
$2,114 42,790 kWh |
$(-860) (-182) MMBtu |
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05: 2.4221 INSTALL COMPRESSOR AIR INTAKES IN COOLEST LOCATIONS |
Savings: $356 Cost: $500 |
$356 | 7,327 | - | - |
$356 7,327 kWh |
- - MMBtu |
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06: 2.3132 RECHARGE BATTERIES ON DURING OFF-PEAK DEMAND PERIODS |
Savings: $446 Cost: - |
$446 | - | - | - |
$446 - kWh |
- - MMBtu |
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07: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $3,012 Cost: $250 |
$3,012 | 60,961 | - | - |
$3,012 60,961 kWh |
- - MMBtu |
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TOTAL RECOMMENDED |
Savings: $13,009 Cost: $2,709 |
$13,869 | 271,688 | $(-860) | (-182) | $13,869 271,688 kWh |
$(-860) (-182) MMBtu |
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TOTAL IMPLEMENTED |
Savings: $4,082 Cost: $250 |
$4,082 | 73,564 | - | - | $4,082 73,564 kWh |
- - MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |