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IAC Assessment: WI0096
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IAC Assessment: WI0096
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IAC Center University of Wisconsin, Milwaukee
Assessment Year 1990
Principal Product AUTOMOTIVE TIRES
NAICS n/a
SIC 3011 - Tires And Inner Tubes
Sales $5,000,000-$10,000,000
# of Employees 60
Plant Area (Sq.Ft.) 0
Annual Production 300,000 Pieces
Production Hrs. Annual 2,375
Location (State) IL
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $149,766 1,456,624 kWh $0.10
Natural Gas $65,912 18,666 MMBtu $3.53
TOTAL ENERGY COSTS $215,678
RECOMMENDED SAVINGS* $120,651 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $15,137
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.3413 BURN FOSSIL FUEL TO PRODUCE STEAM TO DRIVE A STEAM TURBINE-GENERATOR AND USE STEAM EXHAUST FOR HEAT Savings:
$77,488
Cost:
$400,000
$97,696 949,883 $(-20,208) (-5,891) - - $97,696
949,883
kWh
$(-20,208)
(-5,891)
MMBtu
-
-
$
02: 2.3131 RESCHEDULE PLANT OPERATIONS OR REDUCE LOAD TO AVOID PEAKS Savings:
$27,714
Cost:
-
$29,139 - - - $(-1,425) - $29,139
-
kWh
-
-
MMBtu
$(-1,425)
-
$
03: 2.7243 IMPROVE AIR CIRCULATION WITH DESTRATIFICATION FANS / OTHER METHODS Savings:
$8,473
Cost:
$3,895
$(-386) (-3,810) $8,859 2,510 - - $(-386)
(-3,810)
kWh
$8,859
2,510
MMBtu
-
-
$
04: 2.3132 RECHARGE BATTERIES ON DURING OFF-PEAK DEMAND PERIODS Savings:
$5,068
Cost:
$800
$5,068 - - - - - $5,068
-
kWh
-
-
MMBtu
-
-
$
05: 2.6121 REDUCE HOT WATER TEMPERATURE TO THE MINIMUM REQUIRED Savings:
$563
Cost:
-
$563 5,569 - - - - $563
5,569
kWh
-
-
MMBtu
-
-
$
06: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$560
Cost:
$500
- - $560 159 - - -
-
kWh
$560
159
MMBtu
-
-
$
07: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$449
Cost:
$1,744
$449 4,396 - - - - $449
4,396
kWh
-
-
MMBtu
-
-
$
08: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$24
Cost:
$14
$24 586 - - - - $24
586
kWh
-
-
MMBtu
-
-
$
09: 2.6232 INSTALL SET-BACK TIMERS Savings:
$160
Cost:
$400
$160 1,465 - - - - $160
1,465
kWh
-
-
MMBtu
-
-
$
10: 2.2511 INSULATE BARE EQUIPMENT Savings:
$152
Cost:
$352
- - $152 43 - - -
-
kWh
$152
43
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$120,651
Cost:
$407,705
$132,713 958,089 $(-10,637) (-3,179) $(-1,425) - $132,713
958,089
kWh
$(-10,637)
(-3,179)
MMBtu
$(-1,425)
-
$
TOTAL IMPLEMENTED Savings:
$15,137
Cost:
$6,953
$5,718 6,741 $9,419 2,669 - - $5,718
6,741
kWh
$9,419
2,669
MMBtu
-
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes