Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
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Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
174
matching recommendationsNAICS | 2123 | Nonmetallic Mineral Mining and Quarrying |
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Row Colors Legend |
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no implementation information |
Implemented |
NOT Implemented |
ID | # | Year | Products | Savings | Cost | Status |
---|---|---|---|---|---|---|
OR0445 # 03 Y:2003 | 03 | 2003 | REDUCE COMBUSTION AIR FLOW TO OPTIMUM | $1,778 | $150 | Implemented |
OR0445 # 04 Y:2003 | 04 | 2003 | UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS | $1,960 | $0 | Not Implemented |
OR0445 # 05 Y:2003 | 05 | 2003 | RESCHEDULE PLANT OPERATIONS OR REDUCE LOAD TO AVOID PEAKS | $1,505 | $0 | Not Implemented |
OR0445 # 06 Y:2003 | 06 | 2003 | OPTIMIZE PLANT POWER FACTOR | $5,690 | $20,000 | Not Implemented |
GT0762 # 01 Y:2003 | 01 | 2003 | CHANGE RATE SCHEDULES OR OTHER CHANGES IN UTILITY SERVICE | $153,000 | $0 | Not Implemented |
GT0762 # 02 Y:2003 | 02 | 2003 | REPAIR AND ELIMINATE STEAM LEAKS | $12,813 | $700 | Implemented |
GT0762 # 03 Y:2003 | 03 | 2003 | INSTALL / REPAIR INSULATION ON STEAM LINES | $12,072 | $1,430 | Implemented |
GT0762 # 04 Y:2003 | 04 | 2003 | USE SYNTHETIC LUBRICANT | $24,255 | $0 | Implemented |
GT0762 # 05 Y:2003 | 05 | 2003 | UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS | $20,544 | $32,000 | Not Implemented |
GT0762 # 06 Y:2003 | 06 | 2003 | UTILIZE DAYLIGHT WHENEVER POSSIBLE IN LIEU OF ARTIFICIAL LIGHT | $2,390 | $0 | Not Implemented |
GT0762 # 07 Y:2003 | 07 | 2003 | REDUCE ILLUMINATION TO MINIMUM NECESSARY LEVELS | $1,070 | $160 | Not Implemented |
GT0762 # 08 Y:2003 | 08 | 2003 | INCREASE AMOUNT OF CONDENSATE RETURNED | $18,580 | $19,500 | Not Implemented |
GT0762 # 09 Y:2003 | 09 | 2003 | MINIMIZE NON-ESSENTIAL MATERIAL IN HEAT TREATMENT PROCESS | $711,000 | $500,000 | Implemented |
GT0762 # 10 Y:2003 | 10 | 2003 | USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS | $126,034 | $1,000,000 | Implemented |
GT0762 # 11 Y:2003 | 11 | 2003 | USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES | $210,205 | $2,700,000 | Not Implemented |
GT0752 # 01 Y:2003 | 01 | 2003 | ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES | $3,786 | $500 | Implemented |
GT0752 # 02 Y:2003 | 02 | 2003 | IMPROVE LUBRICATION PRACTICES | $3,514 | $0 | Not Implemented |
GT0752 # 03 Y:2003 | 03 | 2003 | MAKE A PRACTICE OF TURNING OFF LIGHTS WHEN NOT NEEDED | $8,459 | $2,000 | Not Implemented |
GT0752 # 04 Y:2003 | 04 | 2003 | COVER OPEN TANKS | $308,000 | $361,000 | Implemented |
GT0752 # 05 Y:2003 | 05 | 2003 | REDUCE COMBUSTION AIR FLOW TO OPTIMUM | $211,700 | $260,000 | Not Implemented |
GT0752 # 06 Y:2003 | 06 | 2003 | ADD/MODIFY EQUIPMENT TO IMPROVE DRYING PROCESS | $1,221,000 | $0 | Not Implemented |
GT0752 # 07 Y:2003 | 07 | 2003 | UPGRADE OBSOLETE EQUIPMENT | $129,140 | $1,200,000 | Implemented |
GT0752 # 08 Y:2003 | 08 | 2003 | USE SMALL NUMBER OF HIGH OUTPUT UNITS INSTEAD OF MANY SMALL INEFFICIENT UNITS | $1,773,429 | $6,000,000 | n/a |
GT0752 # 09 Y:2003 | 09 | 2003 | USE A FOSSIL FUEL ENGINE TO COGENERATE ELECTRICITY OR MOTIVE POWER; AND UTILIZE HEAT | $435,100 | $2,070,000 | Not Implemented |