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IAC Assessment: AM0134
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IAC Assessment: AM0134
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IAC Center Texas A&M, College Station
Assessment Year 1991
Principal Product SANFORIZED COTTON
NAICS n/a
SIC 2211 - Broadwoven Fabric Mills, Cotton
Sales $50,000,000-$100,000,000
# of Employees 320
Plant Area (Sq.Ft.) 0
Annual Production 20,600,000 Pounds
Production Hrs. Annual 6,600
Location (State) TX
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $1,320,682 34,415,299 kWh $0.04
Natural Gas $444,748 169,927 MMBtu $2.62
TOTAL ENERGY COSTS $1,765,430
RECOMMENDED SAVINGS* $185,847 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* -
#|Description Savings
Cost
Status Electricity Usage Natural Gas Other Energy Administrative Changes Electricity Usage Natural Gas Other Energy Administrative Changes
$ kWh $ MMBtu $ MMBtu $ $
01: 2.3192 USE FOSSIL FUEL POWERED GENERATOR DURING PEAK DEMAND PERIODS Savings:
$91,770
Cost:
-
$110,470 - - - $(-18,700) (-2,110) - - $110,470
-
kWh
-
-
MMBtu
$(-18,700)
(-2,110)
MMBtu
-
-
$
02: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$6,677
Cost:
$7,240
$6,677 172,919 - - - - - - $6,677
172,919
kWh
-
-
MMBtu
-
-
MMBtu
-
-
$
03: 2.4239 ELIMINATE OR REDUCE COMPRESSED AIR USAGE Savings:
$18,080
Cost:
$43,900
$18,080 785,463 - - - - - - $18,080
785,463
kWh
-
-
MMBtu
-
-
MMBtu
-
-
$
04: 2.2443 RE-USE OR RECYCLE HOT OR COLD PROCESS EXHAUST AIR Savings:
$29,000
Cost:
$114,000
- - $29,000 11,100 - - - - -
-
kWh
$29,000
11,100
MMBtu
-
-
MMBtu
-
-
$
05: 2.2612 USE COOLING TOWER WATER INSTEAD OF REFRIGERATION Savings:
$14,690
Cost:
-
$14,690 410,317 - - - - - - $14,690
410,317
kWh
-
-
MMBtu
-
-
MMBtu
-
-
$
06: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$10,610
Cost:
-
$12,400 320,926 - - - - $(-1,790) - $12,400
320,926
kWh
-
-
MMBtu
-
-
MMBtu
$(-1,790)
-
$
07: 2.3131 RESCHEDULE PLANT OPERATIONS OR REDUCE LOAD TO AVOID PEAKS Savings:
$11,610
Cost:
-
$11,610 - - - - - - - $11,610
-
kWh
-
-
MMBtu
-
-
MMBtu
-
-
$
08: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$3,410
Cost:
$3,820
$3,410 88,511 - - - - - - $3,410
88,511
kWh
-
-
MMBtu
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$185,847
Cost:
$168,960
$177,337 1,778,136 $29,000 11,100 $(-18,700) (-2,110) $(-1,790) - $177,337
1,778,136
kWh
$29,000
11,100
MMBtu
$(-18,700)
(-2,110)
MMBtu
$(-1,790)
-
$
TOTAL IMPLEMENTED Savings:
-
Cost:
-
- - - - - - - - -
-
kWh
-
-
MMBtu
-
-
MMBtu
-
-
$
Savings
Cost
$ kWh $ MMBtu $ MMBtu $ $
Electricity Usage Natural Gas Other Energy Administrative Changes Electricity Usage Natural Gas Other Energy Administrative Changes