Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Georgia Institute of Technology |
---|---|
Assessment Year | 1989 |
Principal Product | PROCESSED MEATS |
NAICS | n/a |
SIC | 2013 - Sausages And Other Prepared Meats |
Sales | $1,000,000-$5,000,000 |
# of Employees | 80 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 2,380,000 Pounds |
Production Hrs. Annual | 2,080 |
Location (State) | GA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $101,789 | 1,271,102 | kWh | $0.08 |
Natural Gas | $36,932 | 6,982 | MMBtu | $5.29 |
TOTAL ENERGY COSTS | $138,721 | |||
RECOMMENDED SAVINGS* | $25,456 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | - |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $6,310 Cost: $13,690 |
$6,310 | 78,839 | - | - | - | - |
$6,310 78,839 kWh |
- - MMBtu |
- - $ |
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02: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $905 Cost: $403 |
$905 | 11,430 | - | - | - | - |
$905 11,430 kWh |
- - MMBtu |
- - $ |
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03: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $5,912 Cost: $4,250 |
$5,912 | 73,857 | - | - | - | - |
$5,912 73,857 kWh |
- - MMBtu |
- - $ |
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04: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $386 Cost: - |
- | - | $686 | 130 | $(-300) | - |
- - kWh |
$686 130 MMBtu |
$(-300) - $ |
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05: 2.3191 USE DEMAND CONTROLLER OR LOAD SHEDDER |
Savings: $11,340 Cost: $9,000 |
$11,340 | 75,029 | - | - | - | - |
$11,340 75,029 kWh |
- - MMBtu |
- - $ |
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06: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $234 Cost: - |
- | - | $534 | 101 | $(-300) | - |
- - kWh |
$534 101 MMBtu |
$(-300) - $ |
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07: 2.2122 INSTALL / REPAIR INSULATION ON CONDENSATE LINES |
Savings: $369 Cost: $850 |
- | - | $369 | 70 | - | - |
- - kWh |
$369 70 MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $25,456 Cost: $28,193 |
$24,467 | 239,155 | $1,589 | 301 | $(-600) | - | $24,467 239,155 kWh |
$1,589 301 MMBtu |
$(-600) - $ |
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TOTAL IMPLEMENTED |
Savings: - Cost: - |
- | - | - | - | - | - | - - kWh |
- - MMBtu |
- - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |