Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Georgia Institute of Technology |
---|---|
Assessment Year | 1991 |
Principal Product | DIMENSION STONE |
NAICS | n/a |
SIC | 3281 - Cut Stone And Stone Products |
Sales | $10,000,000-$50,000,000 |
# of Employees | 72 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 41,400 Tons |
Production Hrs. Annual | 2,040 |
Location (State) | GA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $531,322 | 6,179,953 | kWh | $0.09 |
Natural Gas | $43,524 | 7,439 | MMBtu | $5.85 |
TOTAL ENERGY COSTS | $574,846 | |||
RECOMMENDED SAVINGS* | $66,921 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $66,921 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $500 Cost: - |
- | - | $800 | 138 | $(-300) | - |
- - kWh |
$800 138 MMBtu |
$(-300) - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 2.2121 INCREASE AMOUNT OF CONDENSATE RETURNED |
Savings: $960 Cost: - |
- | - | $960 | 165 | - | - |
- - kWh |
$960 165 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.2122 INSTALL / REPAIR INSULATION ON CONDENSATE LINES |
Savings: $158 Cost: $289 |
- | - | $158 | 27 | - | - |
- - kWh |
$158 27 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
04: 2.3131 RESCHEDULE PLANT OPERATIONS OR REDUCE LOAD TO AVOID PEAKS |
Savings: $37,560 Cost: - |
$37,560 | - | - | - | - | - |
$37,560 - kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
05: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $183 Cost: - |
$238 | 2,931 | - | - | $(-55) | - |
$238 2,931 kWh |
- - MMBtu |
$(-55) - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
06: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $3,110 Cost: $3,441 |
$3,110 | 38,980 | - | - | - | - |
$3,110 38,980 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
07: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $17,900 Cost: $4,800 |
$17,900 | 223,916 | - | - | - | - |
$17,900 223,916 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
08: 2.6221 USE MOST EFFICIENT EQUIPMENT AT IT'S MAXIMUM CAPACITY AND LESS EFFICIENT EQUIPMENT ONLY WHEN NECESSARY |
Savings: $6,550 Cost: $500 |
$6,550 | 81,770 | - | - | - | - |
$6,550 81,770 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $66,921 Cost: $9,030 |
$65,358 | 347,597 | $1,918 | 330 | $(-355) | - | $65,358 347,597 kWh |
$1,918 330 MMBtu |
$(-355) - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: $66,921 Cost: $9,030 |
$65,358 | 347,597 | $1,918 | 330 | $(-355) | - | $65,358 347,597 kWh |
$1,918 330 MMBtu |
$(-355) - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |