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IAC Assessment: OR0129
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IAC Assessment: OR0129
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IAC Center Oregon State University
Assessment Year 1991
Principal Product DIMENSIONAL LUMBER
NAICS n/a
SIC 2421 - Sawmills And Planing Mills, General
Sales $10,000,000-$50,000,000
# of Employees 125
Plant Area (Sq.Ft.) 0
Annual Production 70,000 Thousand Feet
Production Hrs. Annual 8,736
Location (State) OR
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $387,248 9,431,126 kWh $0.04
Wood $330,572 483,630 MMBtu $0.68
TOTAL ENERGY COSTS $717,820
RECOMMENDED SAVINGS* $103,284 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $103,284
#|Description Savings
Cost
Status Electricity Usage Wood Administrative Changes Electricity Usage Wood Administrative Changes
$ kWh $ MMBtu $ $
01: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$1,102
Cost:
-
$1,102 23,154 - - - - $1,102
23,154
kWh
-
-
MMBtu
-
-
$
02: 2.3131 RESCHEDULE PLANT OPERATIONS OR REDUCE LOAD TO AVOID PEAKS Savings:
$4,277
Cost:
-
$10,517 - - - $(-6,240) - $10,517
-
kWh
-
-
MMBtu
$(-6,240)
-
$
03: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$19,236
Cost:
$30,000
- - $19,236 28,141 - - -
-
kWh
$19,236
28,141
MMBtu
-
-
$
04: 2.7111 REDUCE ILLUMINATION TO MINIMUM NECESSARY LEVELS Savings:
$1,626
Cost:
-
$1,381 33,705 - - $245 - $1,381
33,705
kWh
-
-
MMBtu
$245
-
$
05: 2.2441 PREHEAT BOILER MAKEUP WATER WITH WASTE PROCESS HEAT Savings:
$3,068
Cost:
$3,066
- - $3,068 4,484 - - -
-
kWh
$3,068
4,484
MMBtu
-
-
$
06: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$1,072
Cost:
-
$1,232 31,946 - - $(-160) - $1,232
31,946
kWh
-
-
MMBtu
$(-160)
-
$
07: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$31,573
Cost:
$40,000
$31,573 779,895 - - - - $31,573
779,895
kWh
-
-
MMBtu
-
-
$
08: 2.1131 REPAIR FAULTY INSULATION IN FURNACES, BOILERS, ETC Savings:
$522
Cost:
$864
- - $522 763 - - -
-
kWh
$522
763
MMBtu
-
-
$
09: 2.2122 INSTALL / REPAIR INSULATION ON CONDENSATE LINES Savings:
$790
Cost:
$1,430
- - $790 1,156 - - -
-
kWh
$790
1,156
MMBtu
-
-
$
10: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$2,172
Cost:
-
$1,615 43,669 - - $557 - $1,615
43,669
kWh
-
-
MMBtu
$557
-
$
11: 2.3212 OPTIMIZE PLANT POWER FACTOR Savings:
$12,146
Cost:
$26,250
$12,146 - - - - - $12,146
-
kWh
-
-
MMBtu
-
-
$
12: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$952
Cost:
$2,150
$952 22,567 - - - - $952
22,567
kWh
-
-
MMBtu
-
-
$
13: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$3,521
Cost:
$15,000
$3,521 87,046 - - - - $3,521
87,046
kWh
-
-
MMBtu
-
-
$
14: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$21,227
Cost:
$64,975
$21,227 647,421 - - - - $21,227
647,421
kWh
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$103,284
Cost:
$183,735
$85,266 1,669,403 $23,616 34,544 $(-5,598) - $85,266
1,669,403
kWh
$23,616
34,544
MMBtu
$(-5,598)
-
$
TOTAL IMPLEMENTED Savings:
$103,284
Cost:
$183,735
$85,266 1,669,403 $23,616 34,544 $(-5,598) - $85,266
1,669,403
kWh
$23,616
34,544
MMBtu
$(-5,598)
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Wood Administrative Changes Electricity Usage Wood Administrative Changes