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IAC Assessment: UD0140
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IAC Assessment: UD0140
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IAC Center University of Dayton
Assessment Year 1984
Principal Product MARGARINE, SHORTENING
NAICS n/a
SIC 2079 - Edible Fats And Oils, Nec
Sales $10,000,000-$50,000,000
# of Employees 168
Plant Area (Sq.Ft.) 0
Annual Production 90,000,000 Pounds
Production Hrs. Annual 2,600
Location (State) OH
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $286,024 5,002,638 kWh $0.06
Natural Gas $279,115 48,317 MMBtu $5.78
TOTAL ENERGY COSTS $565,139
RECOMMENDED SAVINGS* $78,274 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $33,545
#|Description Savings
Cost
Status Electricity Usage Natural Gas Electricity Usage Natural Gas
$ kWh $ MMBtu
01: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$947
Cost:
$1,280
$947 14,947 - - $947
14,947
kWh
-
-
MMBtu
02: 2.2522 ISOLATE HOT OR COLD EQUIPMENT Savings:
$2,075
Cost:
$1,240
$858 30,481 $1,217 212 $858
30,481
kWh
$1,217
212
MMBtu
03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$2,348
Cost:
$708
$2,705 27,550 $(-357) (-62) $2,705
27,550
kWh
$(-357)
(-62)
MMBtu
04: 2.2511 INSULATE BARE EQUIPMENT Savings:
$21,331
Cost:
$10,185
$2,870 50,117 $18,461 3,217 $2,870
50,117
kWh
$18,461
3,217
MMBtu
05: 2.2121 INCREASE AMOUNT OF CONDENSATE RETURNED Savings:
$3,213
Cost:
$3,000
- - $3,213 560 -
-
kWh
$3,213
560
MMBtu
06: 2.1224 REPLACE BOILER Savings:
$40,533
Cost:
$25,000
- - $40,533 7,064 -
-
kWh
$40,533
7,064
MMBtu
07: 3.4115 RECOVER AND REUSE COOLING WATER Savings:
$1,755
Cost:
-
$1,755 30,188 - - $1,755
30,188
kWh
-
-
MMBtu
08: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT Savings:
$983
Cost:
$1,500
- - $983 171 -
-
kWh
$983
171
MMBtu
09: 2.3131 RESCHEDULE PLANT OPERATIONS OR REDUCE LOAD TO AVOID PEAKS Savings:
$5,089
Cost:
$3,000
$5,089 - - - $5,089
-
kWh
-
-
MMBtu
TOTAL RECOMMENDED Savings:
$78,274
Cost:
$45,913
$14,224 153,283 $64,050 11,162 $14,224
153,283
kWh
$64,050
11,162
MMBtu
TOTAL IMPLEMENTED Savings:
$33,545
Cost:
$16,413
$14,224 153,283 $19,321 3,367 $14,224
153,283
kWh
$19,321
3,367
MMBtu
Savings
Cost
$ kWh $ MMBtu
Electricity Usage Natural Gas Electricity Usage Natural Gas