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IAC Assessment: WI0050
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IAC Assessment: WI0050
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IAC Center University of Wisconsin, Milwaukee
Assessment Year 1989
Principal Product ICE CREAM
NAICS n/a
SIC 2024 - Ice Cream And Frozen Desserts
Sales $10,000,000-$50,000,000
# of Employees 150
Plant Area (Sq.Ft.) 0
Annual Production 8,000 Thousand Gallons
Production Hrs. Annual 4,125
Location (State) WI
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $394,410 7,760,551 kWh $0.05
Natural Gas $33,233 8,340 MMBtu $3.98
TOTAL ENERGY COSTS $427,643
RECOMMENDED SAVINGS* $27,580 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* -
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.4312 IMPROVE LUBRICATION PRACTICES Savings:
$4,124
Cost:
-
$4,124 81,184 - - - - $4,124
81,184
kWh
-
-
MMBtu
-
-
$
02: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$821
Cost:
-
$821 16,120 - - - - $821
16,120
kWh
-
-
MMBtu
-
-
$
03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$84
Cost:
$713
$84 1,758 - - - - $84
1,758
kWh
-
-
MMBtu
-
-
$
04: 2.2621 MODIFY REFRIGERATION SYSTEM TO OPERATE AT A LOWER PRESSURE Savings:
$9,651
Cost:
-
$9,651 189,918 - - - - $9,651
189,918
kWh
-
-
MMBtu
-
-
$
05: 2.3191 USE DEMAND CONTROLLER OR LOAD SHEDDER Savings:
$2,920
Cost:
-
$3,720 - - - $(-800) - $3,720
-
kWh
-
-
MMBtu
$(-800)
-
$
06: 2.3132 RECHARGE BATTERIES ON DURING OFF-PEAK DEMAND PERIODS Savings:
$3,290
Cost:
$6,000
$3,290 - - - - - $3,290
-
kWh
-
-
MMBtu
-
-
$
07: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$325
Cost:
$500
- - $325 82 - - -
-
kWh
$325
82
MMBtu
-
-
$
08: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT Savings:
$957
Cost:
$5,000
- - $957 240 - - -
-
kWh
$957
240
MMBtu
-
-
$
09: 2.2447 HEAT WATER WITH EXHAUST HEAT Savings:
$5,408
Cost:
$10,000
- - $5,408 1,359 - - -
-
kWh
$5,408
1,359
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$27,580
Cost:
$22,213
$21,690 288,980 $6,690 1,681 $(-800) - $21,690
288,980
kWh
$6,690
1,681
MMBtu
$(-800)
-
$
TOTAL IMPLEMENTED Savings:
-
Cost:
-
- - - - - - -
-
kWh
-
-
MMBtu
-
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes