Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Georgia Institute of Technology |
---|---|
Assessment Year | 1985 |
Principal Product | CARPET DYEING |
NAICS | n/a |
SIC | 2273 - Carpets And Rugs |
Sales | $10,000,000-$50,000,000 |
# of Employees | 135 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 36,000,000 Pounds |
Production Hrs. Annual | 6,120 |
Location (State) | GA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $341,138 | 7,961,899 | kWh | $0.04 |
Natural Gas | $2,743,687 | 595,226 | MMBtu | $4.61 |
Fuel Oil #6 | $91,584 | 18,483 | MMBtu | $4.96 |
TOTAL ENERGY COSTS | $3,176,409 | |||
RECOMMENDED SAVINGS* | $765,729 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | $308,729 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $2,550 Cost: $2,883 |
$2,550 | 59,789 | - | - |
$2,550 59,789 kWh |
- - MMBtu |
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02: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $979 Cost: $820 |
$979 | 22,860 | - | - |
$979 22,860 kWh |
- - MMBtu |
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03: 2.5123 REDUCE FLUID FLOW RATES |
Savings: $10,900 Cost: $25,000 |
- | - | $10,900 | 2,430 |
- - kWh |
$10,900 2,430 MMBtu |
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04: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $17,100 Cost: $800 |
- | - | $17,100 | 3,810 |
- - kWh |
$17,100 3,810 MMBtu |
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05: 2.1232 KEEP BOILER TUBES CLEAN |
Savings: $40,100 Cost: $50,000 |
- | - | $40,100 | 8,930 |
- - kWh |
$40,100 8,930 MMBtu |
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06: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT |
Savings: $99,000 Cost: $120,000 |
- | - | $99,000 | 22,100 |
- - kWh |
$99,000 22,100 MMBtu |
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07: 2.2444 USE HOT PROCESS FLUIDS TO PREHEAT INCOMING PROCESS FLUIDS |
Savings: $191,000 Cost: $150,000 |
- | - | $191,000 | 42,560 |
- - kWh |
$191,000 42,560 MMBtu |
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08: 2.2121 INCREASE AMOUNT OF CONDENSATE RETURNED |
Savings: $156,100 Cost: $82,500 |
- | - | $156,100 | 34,760 |
- - kWh |
$156,100 34,760 MMBtu |
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09: 2.5191 MODIFY DYE BECK |
Savings: $146,000 Cost: $45,000 |
- | - | $146,000 | 32,500 |
- - kWh |
$146,000 32,500 MMBtu |
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10: 2.1111 CONTROL PRESSURE ON STEAMER OPERATIONS |
Savings: $102,000 Cost: $7,000 |
- | - | $102,000 | 22,800 |
- - kWh |
$102,000 22,800 MMBtu |
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TOTAL RECOMMENDED |
Savings: $765,729 Cost: $484,003 |
$3,529 | 82,649 | $762,200 | 169,890 | $3,529 82,649 kWh |
$762,200 169,890 MMBtu |
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TOTAL IMPLEMENTED |
Savings: $308,729 Cost: $106,503 |
$3,529 | 82,649 | $305,200 | 68,040 | $3,529 82,649 kWh |
$305,200 68,040 MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |