Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Massachusetts |
---|---|
Assessment Year | 1992 |
Principal Product | SMALL HARDWARE ITEMS |
NAICS | n/a |
SIC | 3545 - Machine Tool Accessories |
Sales | $5,000,000-$10,000,000 |
# of Employees | 55 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 55,000,000 Pieces |
Production Hrs. Annual | 2,125 |
Location (State) | CT |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $163,091 | 1,473,623 | kWh | $0.11 |
Natural Gas | $25,726 | 3,673 | MMBtu | $7.00 |
Fuel Oil #4 | $57,514 | 13,069 | MMBtu | $4.40 |
TOTAL ENERGY COSTS | $246,331 | |||
RECOMMENDED SAVINGS* | $14,225 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | - |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Fuel Oil #4 | Administrative Changes | Electricity Usage | Natural Gas | Fuel Oil #4 | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.6241 REDUCE TEMPERATURE OF PROCESS EQUIPMENT WHEN ON STANDBY |
Savings: $8,134 Cost: - |
- | - | $8,134 | 1,162 | - | - | - | - |
- - kWh |
$8,134 1,162 MMBtu |
- - MMBtu |
- - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 2.1331 BURN A LESS EXPENSIVE GRADE OF FUEL |
Savings: $3,084 Cost: - |
- | - | $(-5,179) | (-1,254) | $8,263 | 1,878 | - | - |
- - kWh |
$(-5,179) (-1,254) MMBtu |
$8,263 1,878 MMBtu |
- - $ |
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03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $487 Cost: - |
$621 | 5,569 | - | - | - | - | $(-134) | - |
$621 5,569 kWh |
- - MMBtu |
- - MMBtu |
$(-134) - $ |
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04: 2.3131 RESCHEDULE PLANT OPERATIONS OR REDUCE LOAD TO AVOID PEAKS |
Savings: $562 Cost: $509 |
$562 | - | - | - | - | - | - | - |
$562 - kWh |
- - MMBtu |
- - MMBtu |
- - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
05: 2.1213 DIRECT WARMEST AIR TO COMBUSTION INTAKE |
Savings: $686 Cost: $2,108 |
- | - | - | - | $686 | 156 | - | - |
- - kWh |
- - MMBtu |
$686 156 MMBtu |
- - $ |
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06: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $584 Cost: - |
$584 | 5,275 | - | - | - | - | - | - |
$584 5,275 kWh |
- - MMBtu |
- - MMBtu |
- - $ |
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07: 2.2122 INSTALL / REPAIR INSULATION ON CONDENSATE LINES |
Savings: $396 Cost: $168 |
- | - | - | - | $396 | 90 | - | - |
- - kWh |
- - MMBtu |
$396 90 MMBtu |
- - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
08: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $292 Cost: $180 |
$292 | 2,638 | - | - | - | - | - | - |
$292 2,638 kWh |
- - MMBtu |
- - MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $14,225 Cost: $2,965 |
$2,059 | 13,482 | $2,955 | (-92) | $9,345 | 2,124 | $(-134) | - | $2,059 13,482 kWh |
$2,955 (-92) MMBtu |
$9,345 2,124 MMBtu |
$(-134) - $ |
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TOTAL IMPLEMENTED |
Savings: - Cost: - |
- | - | - | - | - | - | - | - | - - kWh |
- - MMBtu |
- - MMBtu |
- - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Fuel Oil #4 | Administrative Changes | Electricity Usage | Natural Gas | Fuel Oil #4 | Administrative Changes |