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IAC Assessment: MA0259
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IAC Assessment: MA0259
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IAC Center University of Massachusetts
Assessment Year 1992
Principal Product SMALL HARDWARE ITEMS
NAICS n/a
SIC 3545 - Machine Tool Accessories
Sales $5,000,000-$10,000,000
# of Employees 55
Plant Area (Sq.Ft.) 0
Annual Production 55,000,000 Pieces
Production Hrs. Annual 2,125
Location (State) CT
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $163,091 1,473,623 kWh $0.11
Natural Gas $25,726 3,673 MMBtu $7.00
Fuel Oil #4 $57,514 13,069 MMBtu $4.40
TOTAL ENERGY COSTS $246,331
RECOMMENDED SAVINGS* $14,225 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* -
#|Description Savings
Cost
Status Electricity Usage Natural Gas Fuel Oil #4 Administrative Changes Electricity Usage Natural Gas Fuel Oil #4 Administrative Changes
$ kWh $ MMBtu $ MMBtu $ $
01: 2.6241 REDUCE TEMPERATURE OF PROCESS EQUIPMENT WHEN ON STANDBY Savings:
$8,134
Cost:
-
- - $8,134 1,162 - - - - -
-
kWh
$8,134
1,162
MMBtu
-
-
MMBtu
-
-
$
02: 2.1331 BURN A LESS EXPENSIVE GRADE OF FUEL Savings:
$3,084
Cost:
-
- - $(-5,179) (-1,254) $8,263 1,878 - - -
-
kWh
$(-5,179)
(-1,254)
MMBtu
$8,263
1,878
MMBtu
-
-
$
03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$487
Cost:
-
$621 5,569 - - - - $(-134) - $621
5,569
kWh
-
-
MMBtu
-
-
MMBtu
$(-134)
-
$
04: 2.3131 RESCHEDULE PLANT OPERATIONS OR REDUCE LOAD TO AVOID PEAKS Savings:
$562
Cost:
$509
$562 - - - - - - - $562
-
kWh
-
-
MMBtu
-
-
MMBtu
-
-
$
05: 2.1213 DIRECT WARMEST AIR TO COMBUSTION INTAKE Savings:
$686
Cost:
$2,108
- - - - $686 156 - - -
-
kWh
-
-
MMBtu
$686
156
MMBtu
-
-
$
06: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$584
Cost:
-
$584 5,275 - - - - - - $584
5,275
kWh
-
-
MMBtu
-
-
MMBtu
-
-
$
07: 2.2122 INSTALL / REPAIR INSULATION ON CONDENSATE LINES Savings:
$396
Cost:
$168
- - - - $396 90 - - -
-
kWh
-
-
MMBtu
$396
90
MMBtu
-
-
$
08: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$292
Cost:
$180
$292 2,638 - - - - - - $292
2,638
kWh
-
-
MMBtu
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$14,225
Cost:
$2,965
$2,059 13,482 $2,955 (-92) $9,345 2,124 $(-134) - $2,059
13,482
kWh
$2,955
(-92)
MMBtu
$9,345
2,124
MMBtu
$(-134)
-
$
TOTAL IMPLEMENTED Savings:
-
Cost:
-
- - - - - - - - -
-
kWh
-
-
MMBtu
-
-
MMBtu
-
-
$
Savings
Cost
$ kWh $ MMBtu $ MMBtu $ $
Electricity Usage Natural Gas Fuel Oil #4 Administrative Changes Electricity Usage Natural Gas Fuel Oil #4 Administrative Changes